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Improvement of No.1 RH Lower Vessel Campaign Life In Kakogawa Works

机译:改善神古川工厂1号RH下容器的运动寿命

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In order to satisfy a request for upgrading steel quality, No.3RH degasser was newly installed at Kakogawa works. After the start of No.3RH operation, the number of heats per day in the existing No.lRH degasser was decreased with an increase in the ratio of high-quality steel which requires long treatment time. With such a great change in service conditions, the campaign life of the No.lRH lower vessel decreased because of the unusual wear of the throat brick. In order to reveal the mechanism of this unusual wear, a stress analysis model of the RH lower vessel refractories was produced and stress analysis was carried out. It was found by means of this analysis that there exists high stress at the problem part of the throat bricks caused by the lack of expansion allowance of the bottom bricks. In order to satisfy the expansion allowance and reduce the stress, the lining of the bottom bricks was improved by using flexible board, and deformation of the bottom shell was controlled. With these improvements, wear of the problem parts decreased remarkably and sudden shut down by troubles has reduced. This paper describes these improvements made on the No.lRH degasser refractories based on stress analysis.
机译:为了满足提高钢质的要求,在神古川工厂新安装了3RH号脱气机。在3RH号开始运行后,现有的1RH号脱气机每天的发热量随着高质量钢比例的增加而减少,这需要较长的处理时间。由于使用条件发生了如此大的变化,由于喉管砖的异常磨损,No.1RH下层容器的使用寿命缩短了。为了揭示这种异常磨损的机理,建立了RH下部容器耐火材料的应力分析模型,并进行了应力分析。通过该分析发现,由于缺乏底部砖的膨胀余量,在喉部砖的问题部分存在高应力。为了满足膨胀余量和减小应力,通过使用柔性板改善了底砖的衬里,并控制了底壳的变形。通过这些改进,问题零件的磨损显着降低,并且因故障而突然停机的情况也有所减少。本文基于应力分析介绍了对1RH型脱气机耐火材料的改进。

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