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Optimization of Solder Volume in Printed Circuit Board Assembly Through an Operating Window Experiment-A Case Study

机译:通过操作窗口实验优化印刷电路板组件中的焊料体积 - 一种案例研究

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摘要

Controlling solder paste volume significantly influences printed circuit board bonding. Applying an improper amount of solder paste during the printing process can cause circuit issues, such as an incomplete circuit with insufficient paste and short circuit with excessive paste. These defects can result in high repair cost or over-usage and wasting of solder paste. Therefore, the appropriate solder paste volume should be determined to ensure the quality of printed circuit board assembly and reduce cost. The solder paste printing problem can neither be classified as larger-the-better, nor smaller-the-better. The problem is a range issue. The operating window is a means to solve such problem. This study applies the operating window methodology to identify an optimal condition to maximize the operating window range. A real case study was presented to confirm the effectiveness of the method. The implementation result achieves a noticeable reduction of 15.9% in the mean usage volume of the solder paste, whereas the standard deviation of the solder volume ratio was reduced by 13.42%. The annual cost saving was expected to reach approximately USD 565,122.
机译:控制焊膏体积显着影响印刷电路板键合。在印刷过程中施加不正当的焊膏量会导致电路问题,例如具有不足的浆料和短路的不完全电路,具有过多的浆料。这些缺陷可能导致高维修成本或过度使用和损坏焊膏。因此,应确定适当的焊膏体积以确保印刷电路板组件的质量并降低成本。焊膏印刷问题既不能被归类为更大的,更好,也不较大。问题是一个范围问题。操作窗口是解决此类问题的手段。本研究适用于操作窗口方法来识别最佳条件以最大化操作窗口范围。提出了一个真正的案例研究以确认该方法的有效性。实施结果在焊膏的平均使用量实现了15.9%的明显减少,而焊料体积比的标准偏差降低了13.42%。预计年度成本节约将达到565,122美元。

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