首页> 外文会议>IEEE Electronics Packaging Technology Conference >Inter-connecting process investigation to resolve delamination
【24h】

Inter-connecting process investigation to resolve delamination

机译:互连过程调查以解决分层

获取原文

摘要

Delamination on the interface between mold compound to die, die paddle and inner leads study has been on-going for quite some time. This is a chronicle defect which will result in electrical continuity failure if delamination penetrates into the interface of mold compound to die surface and mold compound to inner leads e.g., delamination on inner leads or die surface to cause wire broken after thermal stress. To resolve delamination, better materials are needed such as Lead frame, die attach and mold compound. Other than that, a process optimization is also a must to achieve delamination free result. The paper portrays the phenomenon of how delamination occurred after improving the BOM e.g., less water absorption and higher adhesion mold compound. During qualification stage, no delamination occurred after thermal stress. But, on mass volume production run, the delamination occurs on inner leads by sampling check. Four “M” Men, Material, Method and Machines are thoroughly checked and compared with its qualification built and mass production run. No difference or conclusion can be observed and made. But, the delamination was there though no finding/difference was observed. However, one conclusion can be made is qualification is small volume but mass confirmation run is large volume. Based on the assumption, Delamination comparison between small volume VS. large volume was conducted to check the difference. Then, the root cause as die attach outgassing to cause contamination on package is observed. The contamination is later turn into delamination after Thermal.
机译:在模塑料与模具,模座和内部引线之间的界面上的脱层研究已经进行了相当长的时间。这是一种长期缺陷,如果分层渗入到模塑料与模具表面之间的界面以及模塑料与内部引线之间的界面中,例如内部引线或模具表面上的分层在热应力作用下导致断线,则将导致电气连续性故障。为了解决分层问题,需要使用更好的材料,例如引线框架,管芯连接和塑封材料。除此之外,实现无分层效果的过程优化也是必须的。本文描述了在改善BOM后如何发生分层的现象,例如,吸水率降低和粘附力增高的模塑料。在鉴定阶段,热应力后不会发生分层。但是,在批量生产过程中,通过采样检查在内部引线上发生分层。彻底检查了四名“ M”型人员,材料,方法和机器,并将其与合格的制造条件和批量生产进行了比较。无法观察和得出任何差异或结论。但是,尽管没有发现/发现差异,但仍存在分层。但是,可以得出的结论是,鉴定量小而批量确认运行量大。根据该假设,小体积VS之间的分层比较。进行大容量检查以检查差异。然后,观察到根本原因,即管芯附着脱气,导致封装上的污染。加热后,污染物会变成分层。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号