首页> 美国政府科技报告 >A study of the possible effect of a thermal post cure on the mechanical properties of the 404 carbon-phenolic ring of the space shuttle solid rocket motor nozzle
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A study of the possible effect of a thermal post cure on the mechanical properties of the 404 carbon-phenolic ring of the space shuttle solid rocket motor nozzle

机译:热后固化对航天飞机固体火箭发动机喷嘴404碳 - 酚环力学性能影响的研究

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Erratic pockets of erosion have occurred on the inner perimeter of the 404 rocket nozzle ring during liftoff firing. It is thought that it may be caused by pockets of volatile matter entrapped during manufacture. A thermal post cure was suggested as a possible means of outgassing such pockets, if they in fact do exist. To confirm an outgassing during a post cure and to establish a working upper temperature limit, thermal gravimetric and differential calorimetric analyses were made on a number of samples from two 404 rings supplied by the manufacturer. Continuous weight loss was observed over the temperature range explored (750 F) indicating outgassing, and a strong exothermic reaction occurs beginning about 390 F. Thus, an upper post cure temperature of 350 F is recommended. To determine the possible effect of a post cure on physical properties, the following tests will be made on matched sets of cured and post cured material: x-radiography (internal structure), linear dimensions, weight, porosity, cross ply thermal expansion, drop and double notch shear strengths, and tensional strength in the ply direction.

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