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Reducing the scrap rate in an electronic manufacturing SME through Lean Six Sigma methodology

机译:通过精益六西格码方法降低电子制造中小企业的报废率

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摘要

Purpose – The aim of this project was to reduce the level of scrap rate in the production of a product known as the “Remote Acceleration Sensor (RAS)” that is used for Air Bags through Lean Six Sigma (LSS) methodology.udDesign/methodology/approach – This is an action research that was conducted in a single case study and used the LSS methodology of DMAIC concentrating on one fully automated sub-process of the production called the “Overmould line”. udFinding – It was found that implementing DMAIC methodology had an effective impact on the production and scrap rate was reduced achieving the 99.03% First Run Yield (FRY) from 98.4% FRY before implementation. This was the improvement from 3.65 to 3.85 in the Sigma scoring term with significant financial impact at this scale. udResearch Limitations/Implications – This action research could be deployed in other sub- processes of the production line, other processes of the company and could also be conducted in more than one single case study from the same sector. The research investigation needs to be fully controlled by the team in order to correctly gauge the effect of any changes made to the process.udPractical Implications – This project adds further evidence of effectiveness of the LSS methodology in manufacturing SMEs through adding value to the process and reducing the scrap rate and waste. The project had greater saving than expected by the managers at £98,000 per annum. This saving could even be higher when the company is expanded. udOriginality/Value- The approach of this research project combines proven statistical tools with some basic but effective lean tools to be applied in an original sequence in order to design robust product and match manufacturing capabilities. udKey Words – Lean Six Sigma, Six Sigma, DMAIC, Manufacturing, SMEs, Scrap Rate
机译:目的–该项目的目的是通过精益六西格码(LSS)方法降低用于气囊的“远程加速度传感器(RAS)”产品的生产中的废品率水平。 udDesign /方法学/方法–这是一项在单个案例研究中进行的行动研究,使用了DMAIC的LSS方法论集中于生产的一个全自动子过程,称为“ Overmould line”。 udFinding –发现实施DMAIC方法对生产产生了有效影响,废品率降低了,从实施前的98.4%FRY达到了99.03%的首次批量生产率(FRY)。这是Sigma评分期内从3.65改善到3.85的结果,在此规模上产生了重大财务影响。 ud研究的局限性/意义–该行动研究可以部署在生产线的其他子流程,公司的其他流程中,也可以在同一行业的多个案例研究中进行。研究调查需要由团队完全控制,以便正确地评估对过程所做的任何更改的影响。 ud实际意义–该项目通过为过程中增加价值,为LSM方法在制造中小企业中的有效性提供了进一步的证据。并减少废品率和浪费。该项目每年节省98,000英镑,超出了管理者的预期。当公司扩展时,这种节省甚至更高。 udOriginality / Value-此研究项目的方法将经过验证的统计工具与一些基本但有效的精益工具结合使用,以按原始顺序进行应用,以设计可靠的产品并匹配制造能力。 ud关键字-精益六西格码,六西格码,DMAIC,制造业,中小企业,废品率

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