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Analysis of Insulation Diagnosis for Generator-Motor Stator Winding and Core in Pumped Storage Power Plants

机译:泵送蓄能电厂发电机电动机定子绕组和芯的绝缘诊断分析

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Since the first pumped storage power plant started operation in South Korea in 1980, 14 generator-motor related failures have occurred, where two of these cases were stator winding failures. This study examines the stator winding failure cases of the "A" pumped storage power generator-motor, which has been operated for more than 30 years, and the "B" pumped storage power generator-motor, which has been operated for more than 20 years. The causes of the failures are analyzed, and their countermeasures are mentioned. Stator rewinding in the "A" pumped storage power plant was performed in 2010 after a winding meltdown caused by a short circuit at the upper side of the phase B stator winding. A ground fault occurred in the "B" pumped storage power plant because of a stator core damage in 2000, where the core clamping force was strengthened, and the stator winding with dielectric breakdown was replaced. Since then, the "A" and "B" pumped storage power plants have been in operation to date through periodic preventive maintenance. In addition to the insulation diagnostic tests of the "B" pumped storage generator-motor performed in the last two years, the correlation between the number as well as the severity of defects through observation of the ultraviolet (UV) rays generated at the winding terminal and the partial discharge (PD) test data were analyzed. Insulation refurbishment was completed for the maintenance of plant B generator-motor No. 2. The quality of the groundwall insulation of stator winding and stator core were also verified by analyzing the results of the off-line PD test and the EL-CID (ELectromagnetic Core Imperfection Detector) test, respectively, before and after the insulation refurbishment.
机译:自1980年首次泵送的存储电厂在韩国开始运行,发生了14个发电机电机相关的故障,其中两种情况下是定子绕组故障。本研究检查了“A”泵送存储发电机 - 电动机的定子绕组故障情况,该电动机已运行超过30岁,“B”泵送存储发电机电动机已被操作超过20年。分析了故障的原因,提到了它们的对策。在通过相位B定子绕组的短路引起的短路引起的绕组熔体之后在2010年进行“A”泵送存储发电厂中的定子卷绕。由于2000年的定子芯损坏,在“B”泵送存储电厂中发生接地断层,其中加强了芯夹紧力,并更换了具有介电击穿的定子绕组。从那时起,通过周期性预防性维护,“A”和“B”泵送存储发电厂已经运作迄今为止。除了在过去两年中执行的“B”泵送存储发生器电动机的绝缘诊断测试之外,通过在绕组端子处产生的紫外线(UV)光线观察紫外线(UV)光线之间的数量与缺陷之间的相关性分析了局部放电(PD)测试数据。为维护厂房B发电机电动机的保养完成了绝缘翻新。通过分析离线PD试验和EL-CID的结果,还验证了定子绕组和定子芯的地下墙隔热的质量(电磁核心缺陷探测器)分别进行绝缘翻新之前和之后。

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