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Liquefaction of improved ground at Port Island, Japan, during the 1995 Hyogoken-nanbu earthquake

机译:在1995年哨兵地震期间,在日本港口岛地震期间改善地面的液化

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Liquefaction at an improved ground in Port Island, a man made island in Japan, during the 1995 Hyogoken-nambu earthquake is presented. The site was improved by the rod compaction method, and neither significant structural damage nor ground deformation was observed at the time of the earthquake. Detailed insitu and laboratory tests were conducted at the site, which included dynamic deformation test and liquefaction strength test of frozen samples. In-situ investigation pointed out that the ground settlement of about 10 cm occurred during the earthquake. Two effective stress earthquake response analyses were conducted using the data from in-situ and laboratory tests. Both calculations showed that the ground near the water table did not liquefy, but the ground 7 meters below the ground surface (4 meters below the water table) liquefied. This result is in consistent witht he observed fact.
机译:在1995年哨兵地震期间,在日本的一个人为岛屿岛港口港口液化地面液化。该部位通过杆压实方法得到改善,在地震时既未观察到显着的结构损坏也没有接地变形。详细的Insitu和实验室测试在该部位进行,其中包括冷冻样品的动态变形试验和液化强度试验。原位调查指出,地震期间发生了约10厘米的地面沉降。使用来自原位和实验室测试的数据进行两种有效的压力地震响应分析。两种计算都表明,水桌附近的地面没有液化,但地面下方7米(4米以下水位下方)液化。这个结果与他观察到的事实一致。

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