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LESSONS LEARNED FROM THE NAIRN AVENUE OVERPASS CONCRETE GIRDER PIER REPAIRS

机译:奈恩大街超载混凝土梁和码头维修的经验教训

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The Nairn Avenue Overpass is a 213 m long, 11-span, 4-lane + sidewalk precast prestressed concrete I-girder bridge over the CP Keewatin Subdivision line in Winnipeg, MB. The superstructure consists of three continuous segments with deck joints at piers #3 and #8. The structure was built in 1967, and underwent major strengthening and rehabilitation of the deck, girders, and bearings in 1985. Piers consist of a cast-in-place pier cap approximately 18 m long supported on two cast-in-place columns approximately 7 to 8 m tall supported on concrete pile caps over timber raft-pile foundations. Leaking omega-style strip seal deck joints at Pier #3 and Pier #8 have exposed the piers and girder ends to chloride contaminated run-off from the deck. In 2002, the pier caps were re-faced on three sides and provided with galvanic anode cathodic protection, and the pier columns received local patch repairs only. In 2014, during a deck rehabilitation project that included rehabilitating the deck joints, Morrison Hershfield (the Consultant) noted significant deterioration of pier column concrete including staining, moderate-to-severe cracking and localized spalling. The Consultant was subsequently engaged by the City of Winnipeg (City) to conduct a field investigation to quantify the degree of deterioration, evaluate alternatives, and undertake design and construction administration of the preferred solution. This presentation describes these steps, and lessons learned from the Contractor, Consultant, and Owner's perspective.
机译:Nairn大道立交桥是一条长213 m的11跨4车道+人行道预制预应力混凝土工字形桥梁,位于MB温尼伯的CP Keewatin细分线上。上层建筑由三个连续的节段组成,在#3和#8墩处有甲板节。该结构始建于1967年,并于1985年对甲板,大梁和轴承进行了大幅度的加固和修复。墩由长约18 m的现浇墩盖组成,支撑在大约7个现浇柱上到8 m高,支撑在木筏基础上的混凝土桩帽上。 3号墩和8号墩处泄漏的欧米茄长条形密封条甲板接头使码头和大梁的末端暴露于甲板上受氯化物污染的径流中。 2002年,墩帽在三个侧面进行了重新修整,并提供了阳极电镀阴极保护,墩柱仅接受了局部修补。 2014年,在包括修复甲板接缝的甲板修复项目中,Morrison Hershfield(顾问)注意到墩柱混凝土的严重劣化,包括染色,中度至重度开裂和局部剥落。随后,该顾问由温尼伯市(市)聘用,进行现场调查,以量化恶化程度,评估替代方案并进行首选解决方案的设计和施工管理。本演示文稿介绍了这些步骤,以及从承包商,顾问和业主的角度汲取的经验教训。

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