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Failure analysis of an aircraft APU exhaust duct flange due to low cycle fatigue at high temperatures

机译:高温下低周疲劳导致飞机APU排气管法兰失效分析

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Considerable crack-like-defects were observed in an auxiliary power unit (APU) exhaust duct flange area in a jet aircraft with 900 cumulative flying hours. A detailed investigation of crack-induced fracture surface was conducted using Scanning Electron Microscopy (SEM) and computer aided thermal-stress analysis. The results showed that failure of the flange occurred due to the combined effects of the flange constraint and the cyclic thermal stress of the duct. The failure analysis in this study calls for the need for improvement in structure design and installation method of the APU duct system in order to reduce the damage resulting from the creep and fatigue crack during the early stages of service.
机译:在累积飞行时间为900个小时的喷气飞机中,在辅助动力装置(APU)排气管法兰区域中观察到了相当大的裂纹状缺陷。使用扫描电子显微镜(SEM)和计算机辅助热应力分析对裂纹引起的断裂表面进行了详细研究。结果表明,法兰失效是由于法兰约束和管道的循环热应力共同作用的结果。本研究中的故障分析要求改进APU管道系统的结构设计和安装方法,以减少在服务初期由于蠕变和疲劳裂纹而造成的损坏。

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