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Strategic steps towards longer and reliable blast furnace trough campaign - Tata Steel experience

机译:延长和可靠的高炉槽运动的战略步骤-塔塔钢铁经验

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摘要

At Tata Steel, Jamshedpur works the hot metal production capacity was enhanced from 3 centre dot 57 mT in 1997-1998 to 5 centre dot 51 mT in 2007-2008 with the same number of cast houses, thereby, increasing the thermal load on the runner system. Maximising trough availability and ensuring zero breakouts were the means to fulfill the objective of handling the increased furnace production. Significant changes in trough refractory design and introduction of new materials like prefabricated shapes helped to improve reliability of the troughs. The paper presents the design and mode of operation of main troughs of different blast furnaces (BFs) operated at Jamshedpur works, modification of trough design in the upgraded G-BF and its performance and details of improvements made in the trough back-up refractory lining, its wear monitoring and cooling systems.
机译:在塔谢钢铁(Tata Steel)的贾姆谢德布尔(Jamshedpur)工厂,在浇铸炉数量相同的情况下,铁水的生产能力从1997-1998年的3个中心点57 mT提高到2007-2008年的5个中心点51 mT,从而增加了流道上的热负荷系统。最大化料槽可用性并确保零中断是实现处理增加的炉产量的目标的手段。槽式耐火材料设计的重大变化和预制形状等新材料的引入有助于提高槽的可靠性。本文介绍了贾姆谢德布尔(Jamshedpur)工厂运行的不同高炉主槽的设计和操作方式,升级的G-BF中槽设计的修改及其性能以及槽后衬耐火炉衬的改进细节,其磨损监测和冷却系统。

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