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Reducing 'Cold Shut' Defects in Horizontal Controlled Flow Pouring Process Aided by Computer Simulation

机译:通过计算机仿真减少水平控制浇注过程中的“冷关”缺陷

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摘要

The mechanism and preventing countermeasures of "cold shut" defect on the surface of a graphite iron casting made by the horizontal controlled flow pouring process have been investigated with the help of computer simulation (Stefan 3D)~1). Foundry rejection due to such kind of defect has been greatly reduced with the optimized gate-system design based on agreements of the simulation and experiments. A semiempirical equation, correlating dimension of the horizontal runner, tilting degrees of the stack mold, upper dimensions of vertical runner and distance in-between them, was proposed as a quick guide of gating system design for this casting process.
机译:借助计算机模拟(Stefan 3D)〜1),研究了通过水平控制浇注工艺在石墨铸铁件表面“冷关”缺陷的发生机理和防止对策。基于仿真和实验的协议,通过优化的浇口系统设计,已大大减少了由于此类缺陷而导致的铸造厂废品率。提出了一个半经验方程,将水平浇道的尺寸,叠层模具的倾斜度,垂直浇道的上部尺寸以及它们之间的距离相关联,以此作为浇铸系统浇铸系统设计的快速指南。

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