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Root Cause Analysis of AC Overcurrent in July 2020 San Fernando Disturbance

机译:7月20日SAN Fernando扰动中AC过流的根本原因分析

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On July 7 2020, approximately 1000 MW reduction in solar photovoltaic (PV) output was experienced by the bulk power system in Southern California after a three-phase fault. Disturbance analysis indicates that instantaneous AC current caused inverter tripping. The projection of the root cause of AC overcurrent from the NERC report is that inverter current control is not tight. This letter provides a quantitative analysis on ac overcurrent and addresses the following questions: (i) what type of current controls may lead to ac overcurrent and (ii) how controller parameters and grid strength may influence ac overcurrent. The letter provides frequency-domain analysis and time-domain simulation results of a grid-integrated inverter to illustrate the effect of control parameters and grid strength on ac overcurrent.
机译:7月7日2020年,在三相故障之后,南加州南部加利福尼亚州散装电力系统经历了大约1000兆瓦的太阳能光伏(PV)输出。 扰动分析表明瞬时交流电流导致逆变器跳闸。 从NERC报告的AC过电流的根本原因的投影是逆变器电流控制不紧。 这封信提供了对AC过电流的定量分析,并解决了以下问题:(i)哪种类型的当前控制可能导致AC过电流和(ii)控制器参数和电网强度如何影响AC过电流。 该字母提供了网格集成逆变器的频域分析和时域仿真结果,以说明控制参数和电网强度对AC过电流的影响。

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