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Failure analysis of IEU drill pipe wash out

机译:IEU钻杆冲洗失败的分析

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Many 127.0X9.19 mm IEU G105 drill pipe failures of wash out occurred after 2367 h of pure drilling time and 8726 m of penetration footage. This paper gives a detailed investigation on these failures and a systematic analysis is carried out on service and loading conditions of the drill pipes. Measurement and inspection were performed on configuration dimensions, chemical composition, mechanical performance, metallography, macro-fractography, micro-fractography, and corrosion products. Configuration stresses at the crack positions of the drill pipe were calculated by FEA. Crack extending velocity of the drill pipe material under corrosion medium was also measured. It is thought from test and analysis results that the drill pipe wash out or fracture accidents were premature corrosion fatigue failure accident. The failure courses were as the following: corrosion pits occurred first on the internal surface at the stress concentrating area of the drill pipe, and then fatigue cracks initiated in pit bottoms, and washed out or fractured subsequently as cracks penetrated through the wall thickness of the drill pipe. The reasons of drill pipe wash out were related to configuration, material quality, and load condition of the drill pipe string.
机译:在2367 h的纯钻井时间和8726 m的钻进距离后,发生了许多127.0X9.19 mm IEU G105钻杆冲刷失败。本文对这些故障进行了详细的调查,并对钻杆的使用和负载情况进行了系统的分析。对外形尺寸,化学成分,机械性能,金相学,宏观形貌,显微形貌和腐蚀产物进行了测量和检查。通过有限元分析计算钻杆裂纹位置处的构型应力。还测量了在腐蚀介质下钻杆材料的裂纹扩展速度。从测试和分析结果可以认为,钻杆冲刷或断裂事故是过早的腐蚀疲劳失效事故。破坏过程如下:首先在钻杆应力集中区域的内表面上出现腐蚀坑,然后在坑底开始产生疲劳裂纹,然后随着裂纹渗透到钻探壁的厚度中而冲掉或破裂。钻杆。钻杆冲刷的原因与钻杆柱的配置,材料质量和负载条件有关。

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