首页> 外文会议>NACE international corrosion conference and expo >Case Study on the Application of Ceramic Coatings to Extend Fired Heater Tube Life and Improving Operational Efficiency with Cost Benefit Analysis
【24h】

Case Study on the Application of Ceramic Coatings to Extend Fired Heater Tube Life and Improving Operational Efficiency with Cost Benefit Analysis

机译:成本效益分析法应用陶瓷涂层延长加热管寿命并提高运营效率的案例研究

获取原文

摘要

The aromatics plant is an important downstream petrochemical unit that produces various aromatic hydrocarbons such as xylenes, benzene, and toluene which are the basic building blocks for production of polyester and polymers resulting in different consumer goods. The heart of aromatics plant is a licensed high-performance Naphtha Reforming unit that operates at low pressure and high temperatures required to promote chemical reactions that improve aromatics production. To achieve the required heat there are 4no. of fired heaters with arbor type coil configuration that raise the feed naphtha temperature to around 545 ℃. The radiant tubes of the heaters are of 9Cr-1Mo (ASTM~((1)) A335 Gr P9) metallurgy with a maximum tube wall temperature of 652 ℃. The tubes are prone to excessive scaling due to high temperature oxidation and scale thickness of up to 1-2mm were found in the tubes. The problem arising due to scaling affect not only the mechanical integrity of the radiant tubes but also lead to multiple operational constraints. The scaling apart from consuming the metal at 0.25 mm/year, acts as an insulator hindering the heat transfer across the tubes, resulting in radiant heat loss and preventing rise of process fluid temperature to desired levels. Moreover, severe scaling also prevents accurate on-stream monitoring of tube skin temperatures. Following a detailed root cause analysis, it was recommended to apply ceramic coating on the radiant tube and extend it to refractory in the furnace box to improve operational and thermal efficiency, while maintaining metallurgical integrity and reliability. Post coating (applied in March 2017), the unit is capable to run at more than 100% at the same heater load with the assurance of long term integrity of heater tubes. The payback from the investment was within 6 months of project execution. This case study, highlights the observations of the radiant tubes along with cost benefit analysis achieved by the application of ceramic coatings to extend tube life and improve operational efficiency.
机译:芳烃厂是重要的下游石化装置,可生产各种芳烃,如二甲苯,苯和甲苯,它们是生产聚酯和聚合物的基本构成要素,从而产生了不同的消费品。芳烃工厂的核心是获得许可的高性能石脑油重整装置,该装置可在低压和高温下运行,以促进化学反应,从而改善芳烃的生产。为了达到所需的热量,有4no。带有心轴型盘管配置的燃烧加热器,将进料石脑油温度提高到545℃左右。加热器的辐射管为9Cr-1Mo(ASTM〜((1))A335 Gr P9)冶金材料,最高管壁温度为652℃。由于高温氧化,该管易于结垢,并且在管中发现高达1-2mm的水垢厚度。由结垢引起的问题不仅影响辐射管的机械完整性,而且导致多种操作限制。除以每年0.25 mm的速度消耗金属之外,结垢还起绝缘子的作用,阻碍了管子间的传热,导致辐射热损失,并防止过程流体温度升高到所需水平。此外,严重的结垢还会妨碍对管道皮肤温度进行准确的在线监测。在进行了详细的根本原因分析后,建议在辐射管上涂覆陶瓷涂层,并将其扩展到炉箱中的耐火材料,以提高操作效率和热效率,同时保持冶金完整性和可靠性。喷涂后(于2017年3月应用),该装置能够在相同的加热器负载下以100%以上的速度运行,并确保了加热器管的长期完整性。投资的回报是在项目执行的6个月内。该案例研究重点介绍了辐射管的观察结果,以及通过应用陶瓷涂层来延长辐射管寿命和提高运营效率而实现的成本效益分析。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号