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Case Study on Preformed Particle Gel for In-depth Fluid Diversion

机译:预成型颗粒凝胶的深入流体导流案例研究

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The paper describes preformed particle gel (PPG) treatments for in-depth fluid diversion in four injection wells located in the north of Lamadian, Daqing oilfield, China. Lamadian is sandstone oilfield with thick net zones. The selected four injectors have 46 connected producers with average water cut of 95.4% before treatment. The paper reports the detailed information for the four well treatments, including well candidate selection criteria, PPG treatment optimization, real-time monitoring result during PPG injection and reservoir performance after treatment. In addition, a discussion is made to analyze why so large amount of large particles can be injected into the reservoir. Large volume of PPG suspension with concentrations of 2,000-2,500 mg/L and particle sizes of 0.06-3.0 mm was injected into each well and it took about 4 months to finish each injection. The injection volume ranges from 11,458 to 17,625 m3 per well with a total of 56,269 m3 of PPG suspension (295,680 lbs of dried PPG) for the four wells. During PPG injection, the increase of the wellhead pressure was quite stable and no PPG was produced from adjacent producers. Recorded real-time monitoring Data about injection pressure and rate, PPG particle size change during PPG injection provide invaluable information to analysis the possibility of fracture/channel in the reservoir. The treatments resulted in an oil increase of 34.8 t/d and average water cut decrease of 0.94% within 10 months after treatments.
机译:本文描述了在中国大庆油田兰德北部的四个注射井中进行了预先形成的颗粒凝胶(PPG)处理。拉米德是砂岩油田,厚网。所选择的四个喷射器具有46个连接的生产商,在治疗前平均水平均降低95.4%。本文报告了四个井处理的详细信息,包括候选较好选择标准,PPG治疗优化,治疗后PPG注射和储层性能期间的实时监测结果。此外,讨论分析为什么可以将大量的大颗粒注入储存器中。浓度为2,000-2,500mg / L和粒度为0.06-3.0mm的大量PPG悬浮液注入每个孔中,每次注射约4个月才能完成。注射体积为每孔11,458至17,625 m 3,总共56,269m 3的PPG悬浮液(295,680磅干燥的PPG)用于四孔。在PPG注射期间,井口压力的增加非常稳定,并且没有从相邻生产商中产生PPG。记录关于注射压力和速率的实时监测数据,PPG注射期间PPG粒度变化提供了可宝贵的信息,以分析水库中骨折/通道的可能性。该治疗导致油增加34.8吨/天,平均水切割在治疗后10个月内减少0.94%。

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