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Evaluation of Heavy Paraffin Solvent Injection in Langgak Oil Field

机译:兰加达油田重型石蜡溶剂注射液评价

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LGK 14 and LGK 25 wells are oil production wells with high paraffin levels. The presence of paraffin around well perforation causes many problems. One of which is a decrease in the rate of production. It solved with rig less workover / well service (WO/WS) is an injection of heavy paraffin solvent. LGK 14 well uses sucker rod pump and LGK 25 uses an electrical submersible pump. Main steps in LGK 14 are injecting heavy parasol, soaking, displacing and producing. The other wells have differences where before the heavy parasol injecting, pump washed first. The challenges are high static bottom hole pressure (SBHP) and fluid reactions. The results show for LGK 14 well decreased oil rate from 25 BOPD to 21.77 BOPD after the heavy parasol injection. LGK 25 well increased the production rate from 21 BOPD to 29.99 BOPD.
机译:LGK 14和LGK 25井是油生产井,具有高石蜡水平。井穿孔周围的石蜡存在导致许多问题。其中一个是生产率下降。它解决了钻机较少的工作服/井服务(WO / WS)是注射重石蜡溶剂。 LGK 14良好使用吸盘杆泵,LGK 25使用电潜水泵。 LGK 14中的主要步骤注射了重阳伞,浸泡,置换和生产。另一个井在重遮阳伞注射之前具有差异,泵首先洗涤。挑战是高静态底部孔压力(SBHP)和流体反应。结果表明,LGK 14重度阳伞注射后21.77 Bopd的油速下降到21.77普波普。 LGK 25从21个Bopd到29.99 Bopd的生产率增加了生产率。

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