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Preliminary Results From a Solvent Gas Injection Field Test in a Depleted Heavy Oil Reservoir

机译:贫油稠油油藏中溶剂气注入现场测试的初步结果

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A field test was run during 1997 and 1998 to collect preliminary data on a solvent gas injection process. The site selected for the test was a "typical" Frog Lake, Alberta, Cummings formation reservoir that had been depleted using PC pump-based cold production methods on both 4 hectare (10 acre) and 8.1 hectare (20 acre) spacing. At the time of solvent injection, area average recovery from the test location was 9.5%, and the existence of wormholes in the reservoir was strongly suggested by regional well-to-well water migration and production of reservoir sand at high initial rates and cumulative volumes. A solvent containing 33 volume % propane and 67 volume % methane was injected at two converted central producers until cumulative volumes of 2 million m~3 and 4 million m~3 were achieved. This paper discusses field observations during the injection, soak, and production periods. A number of circumstances contributed to a poor economic result, but the operational and technical information obtained should prove helpful to operators considering application of, solvent injection processes.
机译:1997年和1998年进行了现场测试,以收集有关溶剂气体注入过程的初步数据。选择进行测试的地点是“典型的”艾伯塔省青蛙湖卡明斯地层储层,该储层已使用基于PC泵的冷生产方法在4公顷(10英亩)和8.1公顷(20英亩)的空间上枯竭。在注入溶剂时,从测试位置的区域平均采收率为9.5%,并且区域性井间水迁移和高初始速率和累积体积的储层砂的产生强烈暗示了储层中存在虫洞。 。在两个转换后的中央生产商处注入含有33%(体积)丙烷和67%(体积)甲烷的溶剂,直到累积体积达到200万立方米和400万立方米。本文讨论了注入,浸泡和生产期间的现场观察。在许多情况下,导致较差的经济结果,但是所获得的操作和技术信息应被证明对考虑应用溶剂注入工艺的操作员有所帮助。

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