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Waste Water Force Main Pipe Construction Alternatives to Protect Existing Foundations in the City of Chandler: Case Study

机译:废水部门主管建设替代品保护钱德勒市的现有基础:案例研究

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To provide additional wastewater capacity and redundancy in South Chandler, Arizona, a new 28" High Density Polyethylene (HDPE) force main was installed from the upsized Kyrene Lift Station three miles east to tie into an existing 66" transmission sewer line. The force main was installed under the State Route Loop 202 (SR 202L) freeway through existing 48" steel casings constructed ten years prior. Additionally, the force main was constructed through a narrow Arizona Department of Transportation (ADOT) corridor, which required clearance from existing utilities, including overhead 69kV power poles. Two locations required innovative solutions to both access the existing sleeves and cross the transmission power pole foundations: 1) crossing of the 69kV power pole required detailed slope stability analysis and location specific trench backfilling; and 2) access to the existing 48" was within 15 feet of an existing ADOT sound wall. Various alternatives for access were analyzed in this paper including temporary shoring, sheet pile installation, and full wall replacement and reconstructing on drilled shafts. Based on the objectives above, the existing power pole does not have sufficient embedment for maximum design loads but is stable with reduced load factors and lower operation wind forces. Also, for construction issue with the existing ADOT sound wall, the temporary shoring and sheet piles used due to the geotechnical conditions and construction costs.
机译:为了在南部钱德勒,亚利桑那州提供额外的废水能力和冗余,新的28“高密度聚乙烯(HDPE)力主要由3英里的升级的Kyrene Lift站安装到位于现有的66”传动下水道线中。通过现有的48“钢外壳在状态路线回路202(SR 202L)高速公路下安装了力主。另外,该力主要通过狭窄的亚利桑那州运输(Adot)走廊构建,这需要清除现有公用事业,包括开销69kV电源极点。两个位置需要创新的解决方案,以进入现有的套管和传输电源领域:1)69kV电源杆的交叉需要详细的斜坡稳定性分析和位置特定沟槽回填;和2)进入现有的48“在现有的Adot声音墙的15英尺范围内。本文分析了各种替代方案,包括临时支撑,薄板安装和钻井轴上的全墙更换和重建。基于上述目的,现有电源杆没有足够的嵌入,用于最大设计负载,但载重因子降低和较低的操作风力稳定。此外,对于现有Adot声墙的施工问题,由于岩土工程和施工成本而使用的临时支撑和薄板桩。

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