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Waste Water Force Main Pipe Construction Alternatives to Protect Existing Foundations in the City of Chandler: Case Study

机译:钱德勒市现有基金会保护废水力量主干管的替代方案:案例研究

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摘要

To provide additional wastewater capacity and redundancy in South Chandler, Arizona, a new 28” High Density Polyethylene (HDPE) force main was installed from the upsized Kyrene Lift Station three miles east to tie into an existing 66” transmission sewer line. The force main was installed under the State Route Loop 202 (SR 202L) freeway through existing 48” steel casings constructed ten years prior. Additionally, the force main was constructed through a narrow Arizona Department of Transportation (ADOT) corridor, which required clearance from existing utilities, including overhead 69 kV power poles. Two locations required innovative solutions to both access the existing sleeves and cross the transmission power pole foundations: 1) crossing of the 69 kV power pole required detailed slope stability analysis and location specific trench backfilling; and 2) access to the existing 48” was within 15 feet of an existing ADOT sound wall. Various alternatives for access were analyzed in this paper including temporary shoring, sheet pile installation, and full wall replacement and reconstructing on drilled shafts. Based on the objectives above, the existing power pole does not have sufficient embedment for maximum design loads but is stable with reduced load factors and lower operation wind forces. Also, for construction issue with the existing ADOT sound wall, the temporary shoring and sheet piles used due to the geotechnical conditions and construction costs.
机译:为了在亚利桑那州南钱德勒提供更多的废水处理能力和冗余,从东三英里的大型Kyrene升降机站安装了一条新的28英寸高密度聚乙烯(HDPE)压力主管,以与现有的66英寸输水排污管线连接。力主通过十年前建造的现有48英寸钢制套管安装在State Route Loop 202(SR 202L)高速公路下方。此外,部队总管是通过狭窄的亚利桑那州交通运输部(ADOT)走廊建造的,该走廊需要与现有公用设施(包括架空的69 kV电线杆)进行清理。两个位置都需要创新的解决方案来访问现有的套管并穿过输电杆的基础:1)跨越69 kV的电源杆需要详细的边坡稳定性分析和特定于位置的沟槽回填; 2)进入现有48英寸的通道距离现有ADOT声墙不到15英尺。本文分析了各种通道的替代方案,包括临时支撑,板桩安装,全壁置换和钻探井的重建。基于上述目标,现有的电线杆没有足够的嵌入物可承受最大的设计负荷,但在降低负荷系数和降低运行风力的情况下却很稳定。此外,对于现有ADOT声墙的施工问题,由于岩土工程条件和施工成本的原因,使用了临时支撑和板桩。

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