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Successful Optimization Strategies Combine to Deliver Significant Performance Boost at the Edge of the ERD Envelope, Sakhalin Island, Russia

机译:成功的优化策略结合在于俄罗斯萨哈林岛的ERD信封边缘提供重大表现提升

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Numerous performance enhancement initiatives were used by the operator for the Sakhalin I project in drilling and completing the world-class extended reach drilling (ERD) program at the Odoptu Field, Sakhalin Island, Russia. As a result of the drilling successes and favorable production performance, the initial seven-well ERD program was expanded to nine wells, including the world record OP-11 well. The operator's philosophy of relentless redesign to remove limiters from the drilling process resulted in significant performance improvements in all areas of drilling and completion operations. This paper provides details and results for many of the key performance initiatives used. Operators are continually striving to drill longer, faster, and at lower costs while minimizing risks to provide maximum shareholder value. During the Odoptu ERD drilling program, a constant progression of performance improvement, time reduction, and dependability strategies were used. These optimization initiatives resulted in significant performance improvements for the project and numerous industry records. The nine Odoptu ERD wells were drilled at a cost below the budgeted amount for the first seven wells. As a result of the initiatives employed, non-productive time (NPT) was reduced from an average of 21% on the first four wells to less than 3% on the last five. Aggressive shock and vibration mitigation efforts through bit redesign, bottomhole assembly (BHA) vibration analysis and operational optimizations resulted in record BHA runs. Wellbore instability issues were successfully mitigated through design and operational practices. Completion practices were high-graded and optimized and as a result, all completions in the long horizontal intervals were successfully placed using partial string rotation techniques. Drilling ERD wells at the edge of industry experience in a cost effective and low-risk manner requires careful attention to detail and a commitment by the operator and contractors to continuously improve.
机译:运营商在钻井和完成Odoptu领域,萨哈林岛,俄罗斯施工时,运营商赛马林I项目的智能队I用于钻探和完成世界级的延长钻井(ERD)计划。由于钻探成功和良好的生产性能,最初的七大井ERD计划扩展到九个井,包括世界纪录OP-11。操作员无情重新设计的哲学,以从钻井过程中删除限制器导致钻井和完成操作的所有领域的显着性能改进。本文提供了许多关键绩效计划的详细信息和结果。运营商不断努力频道更长,更快,更低的成本,同时最大限度地降低风险,以提供最大的股东价值。在Odoptu ERD钻探计划期间,使用了恒定的性能改善,减少时间和可靠性策略的进展。这些优化举措导致该项目和众多行业记录的显着改进。九个Odoptu ERD井被钻取,低于前七个井的预算金额。由于采用的举措,非生产时间(NPT)在前四个井中的平均值降低了21%,而最后五个井中的少于3%。通过钻头重新设计,井底组装(BHA)振动分析和操作优化产生了积极的冲击和减振力,导致记录BHA运行。通过设计和运营实践成功减轻了Wellbore不稳定问题。完成实践是高分级和优化的,因此,使用部分串旋转技术成功放置了长水平间隔的所有完成。钻井ERD井以成本效益,低风险的方式,需要仔细关注经营者和承包商不断改进的细节和承诺。

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