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Revival of Mumbai High North - A Case Study

机译:孟买高北复兴 - 以案例研究

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Mumbai High located about 160 km West-North-West of Mumbai City in the Arabian Sea is the largest offshore field in India. The field is being produced through 7 process and 110 well platforms. On 27th July 2005, an unfortunate accident at one of Mumbai High platforms i.e. BHN platform, resulted in devastating fire. This resulted in complete damage to BHN process platform, damage to nearby process platform NF and moderate damage to the well-cum-process-platform NA & gas-compressor-cum-water injection platform- MNW. The accident was caused by the impact of an approaching Multi support vessel in the hostile monsoon weather. The accident caused major disruption of offshore production systems of Mumbai High field. Multi disciplinary teams (MDTs) were constituted for planning, executing, coordinating and monitoring the tasks with active support from offshore field personnel and contractors with the objective to restore production, water injection, gas production in shortest possible time. The offshore management team systematically devised and executed revival plans for restoring Mumbai High North field production of 105,000 b/d with 4 MM m3/d gas. The Revival plans envisaged short term, medium term and long term actions. The short term actions were planned for 2 months, medium term actions for 6 months and long term actions for more than 2 year period. Based on systematic actions, 85% of Mumbai High North oil and gas production was restored within 30 days. Oil production from nearby NQO process complex and 5 well platforms of BHN was revived under structured plan to bring the field back to normalcy. The total field production could be restored to a level of 235000 vis-à-vis 265000 b/d at pre-accident levels withn 6 months. The paper describes about the accident and sequential actions for restoration of production which were planned and executed with precision.^
机译:Mumbai High位于阿拉伯海的孟买市西北大约160公里,是印度最大的离岸领域。该领域正在通过7过程和110井平台生产。 2005年7月27日,孟买高平台之一的不幸事故是Bhn平台,导致火灾毁灭性。这导致BHN工艺平台完全损坏,附近的过程平台NF和适度损坏的井 - CUM-PROCED-PLADIG-PLATFICH-CUM-CUM-RIMPLY平台 - MNW。事故是由接近的多支撑船在敌对季风天气中的影响引起的。事故引起了孟买高场海外生产系统的重大中断。多学科团队(MDTS)由近海现场人员和承包商的积极支持,以恢复生产,注水,燃气产量在最短的时间内进行规划,执行,协调和监测任务。离岸管理团队系统地设计和执行的复兴计划,以恢复孟买高北野生产105,000平方米的天然气。复兴计划设想短期,中期和长期行动。计划短期措施2个月,中期行动6个月和长期行动超过2年。基于系统行动,85%的孟买高北石油和天然气生产在30天内恢复。在建筑计划下,附近的NQO流程复合体和5个BHN平台的石油产量恢复了将场地恢复为正常。在6个月的情况下,可以在事故前水平处恢复到235000令左右的235000 Vis-à-v的水平。本文介绍了用于恢复生产的事故和顺序动作,这些动作是用精度计划和执行的。^

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