首页> 外文会议>Annual American Astronautical Society Rocky Mountain Guidance and Control Conference >ANOMALISTIC DISTURBANCE TORQUES DURING THE ENTRY PHASE OF THE MARS EXPLORATION ROVER MISSIONSA TELEMETRY AND MARS-SURFACE INVESTIGATION
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ANOMALISTIC DISTURBANCE TORQUES DURING THE ENTRY PHASE OF THE MARS EXPLORATION ROVER MISSIONSA TELEMETRY AND MARS-SURFACE INVESTIGATION

机译:在火星勘探中搬迁迁移阶段的异常干扰扭矩遥测和火星表面调查

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Shortly after landing on Mars, post-flight analysis of the "Spirit" entry data sug gested that the vehicle experienced large, anomalistic oscillations in angle-of-attack starting at about M = 6. Similar analysis for "Opportunity" found even larger oscillations starting immediately after maximum dynamic pressure at M = 14. Where angles-of-attack of 1-2 degrees were expected from maximum dynamic pressure to drogue deployment, the reconstructions suggested 4 to 9 degrees. The next Mars lander, 2007 Phoenix project, was concerned enough to recommend further exploration of the anomalies. Detailed analysis of "Opportu nity" data found significant anomalies in the hypersonic aerodynamic torques. The analysis showed that these torques were essentially fixed in the spinning vehicle. Nearly a year after landing, the "Opportunity" rover took pictures of its aeroshell on the surface, which showed that portions of the aeroshell thermal blanket assembly still remained. This blanket assembly was supposed to burn off very early in the entry. An analysis of the aeroshell photographs led to an esti mate of the aerodynamic torques that the remnants could have produced. A comparison of two estimates of the aerodynamic torque perturbations (one ex tracted from telemetry data and the other from Mars surface photographs) showed exceptional agreement. Trajectory simulations using a simple data de rived torque perturbation model provided rigid body motions similar to that ob served during the "Opportunity" entry. Therefore, the case of the anomalistic at titude behavior for the "Opportunity" EDL is now considered closed and a suggestion is put forth that a similar event occurred for the "Spirit" entry as well.
机译:登陆火星后不久,“精神”入境数据苏格的航班分析涉及车辆经历了大的,异常振荡,在大约M = 6开始的角度开始。“机会”类似的分析甚至更大的振荡在M = 14的最大动态压力之后立即开始。如果预期1-2度的角度,从最大动态压力到滴注部署,则建议建议4到9度。下一个火星着陆器,2007年凤凰项目,足以建议进一步探索异常。详细分析“机会”数据在超音速空气动力学扭矩中发现了显着的异常。分析表明,这些扭矩基本上在纺纱车辆中固定。降落后近一年,“机遇”罗孚在地表上拍摄了空气的照片,这表明空气毛毯组件的部分仍然保持依赖。这种毯子组件应该在入口处很早烧掉。对气动拍摄的分析导致了残余物可以产生的空气动力学扭矩的esti配偶。对空气动力扭矩扰动的两个估计的比较(从遥测数据和来自火星表面照片的另一个遥控器中的一个例子)显示出特殊协议。轨迹模拟使用简单的数据de rived扭矩扰动模型提供了类似于在“机会”条目期间服务的刚体运动。因此,现在被认为是“机会”EDL的施力行为的异常行为的情况,并提出了一个类似的事件发生了“精神”进入的建议。

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