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Case study: Damaging effects of increasing the installed capacity in an existing hydropower plant

机译:案例研究:增加现有水电站装机容量的破坏性影响

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This paper presents a case study of the 960 MW Tonstad hydropower plant, in which the installed capacity was increased from 640 to 960 MW in 1988. In combination with installing new turbine governors, this upgrade resulted in several problems due to higher water discharge and amplified hydraulic transients. Due to high headloss, rapid change of produced power, or a combination of these, free surface flow occurred in a sand trap and flushed sand, gravel and rocks down into the turbines. In addition, high pressure on the downstream side of the reservoir intake gates is observed and has caused uncertainty regarding the structural safety of the gate frames and blades. These problems have resulted in restrictions on operation, and economical loss due to repair and reduced power production revenue. In this work, the layout of the power plant and an analysis of the incidents are presented, and a discussion on how this situation could occur and how it can be avoided in other power plants is conducted. It is concluded that in hydropower plants with complex tunnel systems, very detailed studies are necessary to understand the hydraulic behaviour and to foresee potential problems.
机译:本文介绍了960 MW Tonstad水电站的案例研究,其中装机容量从1988年从640增加到960 MW。与安装新的涡轮机调速器相结合,这一升级导致了由于较高的排水和放大了几个问题液压瞬变。由于高头划线,产生功率的快速变化,或者这些组合,在砂阱和冲洗沙子,砾石和岩石中发生的自由表面流动进入涡轮机。此外,观察到储层进气门的下游侧的高压,并对栅极框架和叶片的结构安全性引起的不确定性。这些问题导致了对运营的限制,以及由于维修和减少电力生产收入而导致的经济损失。在这项工作中,提出了发电厂的布局和对事件的分析,并讨论如何发生这种情况以及如何在其他发电厂中避免。结论是,在具有复杂隧道系统的水电站,有必要非常详细的研究来了解液压行为和预见潜在的问题。

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