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COMBUSTION SYSTEM DEVELOPMENT AND TESTING FOR MAN'S NEW INDUSTRIAL GAS TURBINES MGT 6100 AND MGT 6200

机译:曼氏新型工业燃气轮机MGT 6100和MGT 6200的燃烧系统开发和测试

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This paper describes the development and test results of the low emission combustion system for the new industrial gas turbines in the 6-7 MW class from MAN Diesel & Turbo. The design of a robust combustion system and the achievement of very low emission targets were the most important design goals of the combustor development. During the design phase, the analysis of the combustor (i.e. burner design, air distribution, liner cooling design) was supported with different CFD tools. This advanced Dry Low Emission can combustion system (ACC) consists of 6 cans mounted externally on the gas turbine. The behavior and performance of a single can sector was tested over a wide load range and with different boundary conditions; first on an atmospheric test rig and later on a high pressure test rig with extensive instrumentation to ensure an efficient test campaign and accurate data. The atmospheric tests showed a very good performance for all combustor parts and promising results. The high pressure tests demonstrated very stable behavior at all operation modes and very low emissions to satisfy stringent environmental requirements. The whole operation concept of the combustion system was tested first on the single-can high pressure test bed and later on twin and single shaft gas turbines at MAN's gas turbine test facility. During the engine tests, the can combustors demonstrated the expected combustion performance under real operation conditions. All emissions and performance targets were fully achieved. On the single shaft engine, the combustors were running with single digit ppm NO_x levels between 50% and 100% load. The validation phase and further optimization of the gas turbines and the engine components are ongoing. The highlights of the development process and results of the combustor and engine tests will be presented and discussed within this paper.
机译:本文介绍了曼柴油机与透平公司用于6-7兆瓦级新型工业燃气轮机的低排放燃烧系统的开发和测试结果。强劲的燃烧系统的设计和极低排放目标的实现是燃烧器发展的最重要的设计目标。在设计阶段,燃烧器的分析(即燃烧器设计,空气分配,衬套冷却设计)得到了不同的CFD工具的支持。这种先进的干式低排放罐燃烧系统(ACC)由外部安装在燃气轮机上的6个罐组成。在宽的负载范围内和不同的边界条件下测试了单个罐头扇区的性能和性能。首先是在大气测试台上,然后是在配有广泛仪器的高压测试台上,以确保有效的测试活动和准确的数据。大气测试表明,所有燃烧室部件的性能都非常好,并且结果令人满意。高压测试表明,在所有操作模式下的行为都非常稳定,并且排放量非常低,可以满足严格的环境要求。首先在单罐高压测试台上测试燃烧系统的整个运行概念,然后在MAN的燃气轮机测试设施上的双轴和单轴燃气轮机上进行测试。在发动机测试期间,罐式燃烧室展示了在实际运行条件下的预期燃烧性能。所有排放量和性能指标均已完全实现。在单轴发动机上,燃烧器以在50%至100%负载之间的个位数ppm NO_x水平运行。燃气轮机和发动机组件的验证阶段和进一步优化正在进行中。本文将介绍和讨论开发过程的重点以及燃烧室和发动机测试的结果。

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