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CASE STUDY ANALYSIS OF PROCESS FAN FAILURE AND BEARING HOUSING/SHAFT DESIGN

机译:过程风扇故障和轴承座/轴设计的案例分析

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An Air Movement and Control Association (AMCA) Arrangement 8 fan handling hot process gas experienced several bearing failures and ultimately a catastrophic failure requiring shutdown of the plant's production. The investigation found that the 1st critical of the fan rotor was too close to the operating speed resulting in excessive bearing loads and short bearing life. Rotor dynamic modeling was used to evaluate a new shaft design. A new shaft and one-piece bearing housing were designed, fabricated and installed, successfully moving the critical speed several hundred RPM above running speed. The new design also provided improved maintainability over commercially available designs, as well as lowering vibration and significantly improving reliability. This article discusses the analysis process, rotor modeling, bearing housing design process, vibration data comparison before and after the new shaft and bearing housing were installed.
机译:空气运动和控制协会(AMCA)的8号风机在处理高温气体时遇到了几次轴承故障,最终发生了灾难性故障,需要关闭工厂的生产。调查发现,风扇转子的第一临界点太接近运行速度,导致轴承负荷过大和轴承寿命短。转子动态建模用于评估新的轴设计。设计,制造和安装了新的轴和一体式轴承箱,使临界转速成功地超出了运行速度数百RPM。新设计还提供了比市售设计更高的可维护性,并降低了振动并显着提高了可靠性。本文讨论了新轴和轴承座安装前后的分析过程,转子建模,轴承座设计过程,振动数据比较。

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