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The Successful Completion of a Lower Tertiary Well with Depleted Zones Utilizing Single Trip Multi-Zone Technology

机译:利用单程多区技术成功完成耗尽区的耗尽孔。

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The Lower Tertiary play in the Gulf of Mexico (GoM) was identified and completion approaches were developed in the early 2000s to address the complexities of the formation. The use of single-trip multi-zone completion technology was identified as a cost-effective solution to the stacked pay and has been applied by many operators in the GoM (Clarkson et al. 2008, Burger et al. 2010, Grigsby et al. 2016). As these fields have matured, some operators have experienced formation pressure depletion in some of the pay intervals within the proposed completion, challenging this common completion method.The nature of a single-trip multi-zone completion dictates 1) all of the zones to be completed are perforated at the same time, and 2) the pressure gradients of these zones are similar enough that the well can be controlled by the well fluids. Early in the planning of this project, several of the zones within the pay interval of the target well were identified as depleted, which could result in fluid-loss-related control issues.This paper will present a revised completion methodology to address the depletion problem. It will focus on the planning process, execution, and results of this type completion. It will review the identification of the problem, the different options identified to solve the problem, the planning that went into the preparation for the completion, the challenges that were seen during the completion process, and the results of the completion.It is believed that although the challenge of depletion within the Lower Tertiary is new to this development, this situation will become more common as the Lower Tertiary fields are produced. It is the hope that this paper will assist the industry in dealing with this challenge.
机译:在墨西哥湾(GOM)下第三该剧被识别并完成了方法在21世纪初开发的解决形成的复杂性。采用单行程多完井技术被认定为具有成本效益的解决方案,以堆叠的工资,并已被许多运营商在墨西哥湾应用(Clarkson等人,2008年,伯格等人。2010年,格雷斯比等人。 2016)。由于这些领域已经成熟,一些运营商已经在一些拟议中完成的薪酬区间的经验丰富的地层压力枯竭,挑战单行程多区域完成使然这个共同完成method.The性质1)所有区域中是完成的同时穿孔,和2)这些区域的压力梯度是相似的足以使井可以通过井流体进行控制。早在该项目的规划,多家被认定为耗尽目标的薪酬区间内的区域,这可能会导致液体损失相关的控制问题。本文将提出修订完成的方法来解决这个问题枯竭。它将侧重于规划过程中,执行和这种类型的完成结果。它会检讨这个问题的鉴定,确定了解决问题的不同选项,即进入了完成编制规划,在完成过程中看到挑战和completion.It的结果认为,虽然下第三系内枯竭的挑战是新的这个发展,为下第三场产生这种情况将变得更加普遍。这是希望本文将帮助该行业在应对这一挑战。

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