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INVESTIGATING ROOT CAUSES OF CATU COMPRESSOR STATION SHUT-DOWN DUE TO HIGH DISCHARGE TEMPERATURE – (PPT)

机译:CATU压缩机站截止的根本原因,由于高放电温度 - (PPT)

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摘要

The dimensioning of a compression plant, and especially for the heat exchangers, must foresee the serving of a higher number of operational points. The maximum admissible temperature for natural gas in pipelines should be more thoroughly considered for new projects involving gas compressor stations, and revised if necessary. The operational teams should participate more effectively since the beginning of any undertaking involving the transport of natural gas, mainly for compressor stations.
机译:压缩厂,特别是对于热交换器的尺寸,必须预见到更高数量的操作点。 管道中天然气的最大可允许温度应更彻底地考虑涉及气体压缩机站的新项目,并在必要时修改。 由于任何涉及自然气体运输的任何承诺的开始,运营团队应更有效地参与,主要用于压缩机站。

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