首页> 外文会议>ITA-AITES World Tunnel Conference; 20050507-12; Istanbul(TR) >Rock reinforcement design for unstable tunnels originally excavated in very poor rock mass
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Rock reinforcement design for unstable tunnels originally excavated in very poor rock mass

机译:最初以极差的岩石质量开挖的不稳定隧道的岩石加固设计

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摘要

Number 7 Malatya railroad tunnel was excavated through the toe of a paleo-landslide material in 1930. Ever since that date, this horseshoe shape tunnel, having width and height of 5 m and 6 m, respectively, struggled with stability problems. A large amount of deformation (170 cm) developing through the years and leading to miss alignment of the tunnel was observed. In this paper, firstly a new approach developed for classifying very poor quality rock mass was presented. Secondly, evaluations were made on the stability of the tunnel. Thirdly, information is provided on rock reinforcement design. Finally, the results of finite element analysis (FEA) conducted for evaluating the stability of unreinforced tunnel and the tunnel reinforced by self drilling anchors (MAI-bolt) designed based on empirical method were given.
机译:马拉蒂7号铁路隧道是在1930年通过古滑坡材料的脚趾开挖的。自那时以来,这条马蹄形隧道的宽度和高度分别为5 m和6 m,一直存在稳定性问题。多年来,观察到大量变形(170厘米),导致隧道未对准。在本文中,首先提出了一种新的方法,用于对质量很差的岩体进行分类。其次,对隧道的稳定性进行了评估。第三,提供有关岩石加固设计的信息。最后,给出了基于经验方法设计的无筋隧道和自钻锚(MAI-bolt)加固隧道稳定性的有限元分析结果。

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