首页> 外文会议>International Symposium on Modern Tunneling Science and Technology (IS-Kyoto 2001), Oct 30-Nov 1, 2001, Kyoto, Japan >A fundamental study on dynamic response of tunnel reinforcement structure for high speed railway
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A fundamental study on dynamic response of tunnel reinforcement structure for high speed railway

机译:高速铁路隧道加固结构动力响应基础研究

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Recently, there have been some reports of deteriorated concrete linings in railroad tunnels. In order to protect train tracks from falling debris, the installation of reinforcement structure is proposed, which makes possible the installation work at night without suspending train services. Therefore, this proposal should assume the situations where the reinforcement structure would be left unfinished by some reason. In this study, a numerical analysis was carried out on the safety of trains passing through the tunnel without backfilling being conducted, using the measurement data of pneumatic pressure fluctuation and vibration. The analysis results confirmed that the proposed reinforcement structure maintains sufficient safety even in an unfinished condition and also suggested that it is desirable to install displacement-restricting spacers on the ends of the structure to prevent vibration.
机译:最近,有一些关于铁路隧道混凝土衬砌变质的报道。为了保护火车轨道免于掉落的杂物,提出了安装加固结构的方法,该加固结构使得在夜​​间进行安装工作而不中断火车服务成为可能。因此,该建议应假设由于某种原因未完成加固结构的情况。在这项研究中,利用气压波动和振动的测量数据,对经过隧道而不经过回填的列车的安全性进行了数值分析。分析结果证实,提出的增强结构即使在未完成的情况下也保持足够的安全性,并且还建议在结构的端部安装位移限制垫片以防止振动。

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