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Improving the Mill Productivity through Technological Interventions at CRM of Rourkela Steel Plant

机译:在Rourkela钢铁厂CRM中通过技术干预提高轧机生产率

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Cold Rolling Mill (CRM) complex of Rourkela Steel Plant (RSP) was set up in 1968. The CRM has two pickling lines which use sulphuric acid as pickling medium. Production level at pickling lines were significantly low as its speed was restricted to 60-70% of its rated value due to inferior quality of HR coil and improper bath conditions. Pickled coils produced at this line were also observed to have inferior surface quality. Cold rolling of these coils at the Tandem Mill with deficient roll cooling system was leading to higher occurrence of strip breakage and inferior shape of the coils. These problems resulted in lower productivity of the cold rolling mill. Various technological measures were taken both at the Pickling Line and at the Tandem Mill to improve their operating conditions. These measures include introduction of improved scale washing system at Pickling Line and heat exchanger in acid regeneration plant to improve pickling bath condition. To address these deficiencies of graphite block heat exchanger, new generation 'tantalum shell and tube heat exchanger' has been introduced in pickling lines. An automatic temperature control system was also designed and installed to control pickling bath temperature within ±2C of the desired bath temperature. Roll cooling system at Tandem Mill was modified to reduce thermal- crown of work rolls at the stands 4 and 5, which helped in improving shape of coils and reducing strip breakages. With these measures, productivity of the cold rolling mill through Pickling Line 2 - Tandem Mill route could be increased by 25-30%. There was also reduction in diversion on account of bad shape of CR coils by about 30%.
机译:Rourkela钢铁厂(RSP)的冷轧厂(CRM)于1968年成立。CRM有两条酸洗线,这些酸洗线使用硫酸作为酸洗介质。酸洗生产线的生产水平非常低,因为由于热轧卷质量低劣和熔池条件不佳,其速度被限制在其额定值的60-70%。还观察到在此生产线上生产的酸洗卷材的表面质量较差。在具有不足的辊式冷却系统的串联轧机上对这些卷进行冷轧导致带材断裂的发生率更高,并且卷材的形状较差。这些问题导致冷轧机的生产率降低。酸洗线和串联轧机都采取了各种技术措施,以改善其工作条件。这些措施包括在酸洗线和酸再生厂的热交换器中引入改进的水垢清洗系统,以改善酸洗液的状况。为了解决石墨块式热交换器的这些缺陷,酸洗生产线引入了新一代的“钽壳管式热交换器”。还设计并安装了自动温度控制系统,以将酸洗槽温度控制在所需槽温度的±2C之内。修改了Tandem轧机的轧辊冷却系统,以减少4号和5号轧机工作辊的热凸度,这有助于改善卷材的形状并减少带钢的断裂。通过这些措施,通过酸洗线2-串联轧机路线的冷轧机的生产率可以提高25-30%。由于CR线圈的不良形状,转移也减少了约30%。

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