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Oxy-gas forehearths: results of mathematical modeling of a flint glass and field trials on a borosilicate glass

机译:氧气前炉:火石玻璃的数学建模结果和硼硅酸盐玻璃的现场试验

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This paper describes the results of mathematical modeling, burner development, and field trials carried out with oxy-gas forehearths. Mathematical modeling was carried out for the rear cooling section of a BH-F forehearth conditioning a flintglass. The modeling coupled the glass channel with the forehearth combustion space. The glass exit temperatures from this section were compared under both air-gas firing and oxy-gas firing. Results indicated that for the same glass flow rates, cooling was more efficient in the center of the channel and heating was more efficient close to the sides under oxy-gas firing. The combined effect was a 30% improvement over air-gas firing in temperature spread at the exit of the cooling zone. Conversely, the modelalso predicted that for similar temperature spreads, oxy-gas firing would allow the pull through the forehearth to be increased by 30%. Special very low-flow oxy-gas burners have been patented for use in forehearth applications. This includes the mantleblocks, quarls, and burners for side-channel applications and bowl/spout applications. A forehearth for the production of borosilicate glass lighting components was successfully converted to oxy-gas firing in 1996. This was done to overcome the problemsexperienced with air-gas firing. Oxygen-gas firing, by reducing the volume flow of combustion gases and increasing the available heat from the fuel, leads to increased output, improved glass quality, and lengthened refractory life. This paper describesthe changes made to the forehearth and the improvements gained in the glass conditioning process. In September 1997, the melter was repaired and the opportunity was taken to make further improvements to the forehearth.
机译:本文介绍了使用氧气前炉进行数学建模,燃烧器开发和现场试验的结果。对BH-F型供料器调节火石的后部冷却部分进行了数学建模。该模型将玻璃通道与前炉燃烧空间结合在一起。比较了在空气燃烧和氧气燃烧下该部分的玻璃出口温度。结果表明,对于相同的玻璃流量,在氧气燃烧下,通道中央的冷却效率更高,靠近侧面的加热效率更高。综合效果是,在冷却区出口处的温度分布比空气燃气燃烧提高了30%。相反,该模型还预测,对于类似的温度分布,氧气燃烧将使通过前炉的拉力增加30%。特殊的超低流量氧气燃烧器已获得专利,可用于前炉应用。其中包括用于边槽应用和碗/水嘴应用的罩块,石英和燃烧器。 1996年,用于生产硼硅酸盐玻璃照明组件的前炉成功地转换为氧气燃烧。这样做是为了克服空气烧结所遇到的问题。通过减少燃烧气体的体积流量并增加燃料的可用热量进行氧气燃烧,可提高产量,改善玻璃质量并延长耐火寿命。本文介绍了对前炉的更改以及玻璃调节过程中获得的改进。 1997年9月,对熔炉进行了维修,并借此机会对前炉进行了进一步改进。

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