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Upgrading the Industrial Process Flowsheet for the Dehydration of Methylbutenes to Isoprene. II: Analysis of Plant Test Results and Industrial Implementation of the Upgraded Design

机译:升级用于将甲基丁烯脱水成异戊二烯的工业工艺流程图。二:工厂测试结果分析和升级设计的工业实施

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Pilot tests of technology for the dehydration of methylbutenes to isoprene are performed in a tworeactor system with an additional supply of an overheated gas into the interreactor space. The tests are performed on a pilot plant with two adiabatic reactors. The total volume of the catalyst charge is 60 dm~3, the temperatures are 565–620℃, the contact time is 0.18–0.25 s, the raw material is diluted with steam in a weight ratio of С_5Н_(10) : Н_2О = 1.0 : (6.0–30.0), and the excess pressure is 0.6–0.7 kgf/cm~2. The dependence of the isoprene concentration in the contact gas on the heat energy supplied by the raw material and steam is determined under conventional conditions of the process and in a pseudo-isothermal mode via an additional supply of overheated gas into the interreactor space. It is shown that the isoprene yield is increased by 10–12% by using the upgraded mode. The conditions for conducting the industrial process are determined based on the obtained results. After upgrading the design, tests are performed at the synthetic rubber factory of PAO Nizhnekamskneftekhim on a plant for the dehydrogenation of methylbutenes in the reactor with a doublelayer catalyst bed (nine tons per layer). The patterns established during the pilot tests generally prove to be true, but the selectivity of the process is reduced due to a number of design flaws. Corrective measures are outlined. Comparison of the experimental results and the calculated values confirm the accuracy of the mathematical model.
机译:在双反应器系统中进行甲基丁烯脱水为异戊二烯的技术的先导测试,并向反应器间空间中额外供应过热气体。测试是在带有两个绝热反应器的中试装置上进行的。催化剂装料的总体积为60 dm〜3,温度为565–620℃,接触时间为0.18–0.25 s,原料用蒸汽稀释,重量比为С_5Н_(10):Н_2О= 1.0 :(6.0-30.0),过压为0.6-0.7 kgf / cm〜2。接触气体中异戊二烯浓度对原料和蒸汽提供的热能的依赖关系,是在该方法的常规条件下并通过伪等温模式通过向反应器间空间中额外供应过热气体来确定的。结果表明,使用升级模式,异戊二烯的产率提高了10–12%。根据获得的结果确定进行工业过程的条件。升级设计之后,在PAO Nizhnekamskneftekhim的合成橡胶工厂进行测试,该工厂用于在带有双层催化剂床(每层9吨)的反应器中对甲基丁烯进行脱氢。在先导测试期间建立的模式通常被证明是正确的,但是由于许多设计缺陷,降低了过程的选择性。概述了纠正措施。实验结果和计算值的比较证实了数学模型的准确性。

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