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Case Study: Mine void investigation and remediation for the West Chariestown Bypass, Newcastle

机译:案例研究:纽卡斯尔西Chariestown绕行的矿空调查和整治

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摘要

The completed West Charlestown Bypass project comprises a 6.5 km length of dual carriageway urban freeway south west of the Newcastle CBD, in New South Wales, Australia. This section of State Highway 23 extends from the Pacific Highway at Windale in the south, to Charlestown Road at Kotara in the north. A 1 km length of the Bypass, at the northern extent of the works, traverses old underground mine workings with overburden depths as shallow as 5 m ranging up to 30 m. The mine workings are within the Australasian Coal Seam and they were undertaken by two collieries, initially in the 1800's by the Australasian Coal Company and later in the early 1900's by the Newcastle Myall Colliery. The presence of these old mine workings and associated subsidence effects posed a difficult problem for the design and construction of the Bypass. The Bypass design was required to be safe and serviceable, considering the potential impact of ongoing mine subsidence associated with these workings. A number of treatment options were considered, with the adopted design including a combination of excavate, collapse and backfill of shallow mine workings, and grouting of voids where the workings were located at greater depths. This paper presents a case study of the pre-construction investigations, including discussion of the methodologies adopted and their success, the design requirements and options considered, and the completed mine void treatment works.
机译:已完成的西查尔斯敦旁路项目包括在澳大利亚新南威尔士州纽卡斯尔CBD西南的一条6.5公里长的双车道城市高速公路。 23号州际公路的这一部分从南部的Windale的太平洋公路延伸到北部的Kotara的Charlestown Road。在工程的北部,绕行道的长度为1公里,横穿覆盖深度达5 m至30 m的覆盖层深度的旧地下矿井。矿山的开采工作在澳大利亚的一个煤层内,由两个煤矿负责,最初是在1800年代由澳大利亚煤炭公司进行的,后来在1900年代初是由纽卡斯尔Myall煤矿进行的。这些老矿山作业的存在和相关的沉陷影响给旁路的设计和施工带来了难题。考虑到与这些作业相关的持续的地雷沉陷的潜在影响,要求旁路设计必须安全且易于维护。考虑了多种处理方案,采用的设计包括浅井巷道的开挖,坍塌和回填以及巷道位于更深处的空隙注浆的组合。本文介绍了施工前调查的案例研究,包括讨论所采用的方法及其成功,设计要求和考虑的方案以及已完成的矿洞处理工作。

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