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A study on the effective management by the quality control technique concerning the PCB detoxification plant

机译:PCB解毒厂的质量控制技术有效管理研究

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This study is on the effective management by the quality control technique concerning the PCB detoxification plant. The DMAIC Method (Define, Measure, Analyze, Improve, and Control) was applied to the actual construction permission procedure for the purpose of shortening of the construction permission period of a PCB detoxification plant. Firstly, the delay of Lead Time (LT), i.e., the duration period of the expert meetings is considered to be a defect in products, and a rate of defect (R%) was defined. Next, based on the failure mode effects analysis, Risk Priority Number (RPN) was calculated and the intensity of impact of the factors, which causes a defect, was evaluated. By execution of actions recommended in order to prevent the risk of the delay of LT, all RPN became less than 120 after the second expert meeting and the third expert meeting became the final meeting. Finally LT, which had required about ten months conventionally, was shortened to 4.5 months, and as a result, R = 15% was obtained. Consequently, although quantification has been considered very difficult in the field of the construction management concerning a project until now, our study showed that this methodology is effective even in that field.
机译:本研究采用了有关PCB解毒厂的质量控制技术的有效管理。为了缩短PCB解毒厂的结构允许期,将DMAIC方法(定义,测量,分析,改进和控制)应用于实际的结构允许程序。首先,延迟时间(LT),即专家会议的持续时间被认为是产品的缺陷,定义了缺陷率(R%)。接下来,基于故障模式效应分析,计算风险优先级(RPN),并评估导致缺陷的因素的影响的强度。通过执行建议的行动,以防止延迟延迟的风险,在第二次专家会议之后,所有RPN都变得小于120,第三次专家会议成为最终会议。最后,常规需要大约十个月的LT缩短至4.5个月,结果,获得r = 15%。因此,尽管在施工管理领域已经被认为是迄今为止的施工管理领域的量化,但我们的研究表明这种方法即使在该领域也是有效的。

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