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A study on the effective management by the quality control technique concerning the PCB detoxification plant

机译:利用PCB排毒厂的质量控制技术进行有效管理的研究。

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摘要

This study is on the effective management by the quality control technique concerning the PCB detoxification plant. The DMAIC Method (Define, Measure, Analyze, Improve, and Control) was applied to the actual construction permission procedure for the purpose of shortening of the construction permission period of a PCB detoxification plant. Firstly, the delay of Lead Time (LT), i.e., the duration period of the expert meetings is considered to be a defect in products, and a rate of defect (R%) was defined. Next, based on the failure mode effects analysis, Risk Priority Number (RPN) was calculated and the intensity of impact of the factors, which causes a defect, was evaluated. By execution of actions recommended in order to prevent the risk of the delay of LT, all RPN became less than 120 after the second expert meeting and the third expert meeting became the final meeting. Finally LT, which had required about ten months conventionally, was shortened to 4.5 months, and as a result, R = 15% was obtained. Consequently, although quantification has been considered very difficult in the field of the construction management concerning a project until now, our study showed that this methodology is effective even in that field.
机译:这项研究是关于PCB排毒工厂的质量控制技术的有效管理。 DMAIC方法(定义,测量,分析,改进和控制)被应用于实际的施工许可程序,目的是缩短PCB排毒工厂的施工许可期限。首先,将提前期(LT)的延迟(即专家会议的持续时间)视为产品缺陷,并定义缺陷率(R%)。接下来,基于故障模式影响分析,计算风险优先级数(RPN),并评估导致缺陷的因素的影响强度。通过执行建议的措施以防止LT延迟的风险,在第二次专家会议和第三次专家会议成为最终会议之后,所有RPN均不足120。最后,通常需要约10个月的LT缩短为4.5个月,结果,R = 15%。因此,尽管到目前为止,在一个项目的施工管理领域中,量化一直被认为是非常困难的,但我们的研究表明,即使在该领域,这种方法也是有效的。

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