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A DMAIC Six Sigma approach to quality improvement in the anodising stage of the amplifier production process

机译:一种DMAIC六西格玛的质量改进方法,放大器生产过程的阳极升高

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Purpose - The purpose of this paper is to study the anodising process of a portable amplifier production process to identify and eliminate the sources of variations, in order to improve the process productivity. Design/methodology/approach - The study employs the define-measure-analyse-improve-control (DMAIC) Six Sigma methodology. Within the DMAIC framework various tools of quality management such as SIPOC analysis, cause and effect diagram, current reality tree, etc., are used in different stages. Findings - High rejection rate was found to be the main problem leading to lower productivity of the process. Four types of defects were identified as main cause of rejections in the baseline process. Pareto analysis resulted in detection of the top defects, which were then analysed in details to find the root cause of the problem. Further study resulted in finding improvement measures that were discussed with the management before implementation. The process is sampled again to check the improvements, and control measures were established. Practical implications - The study provides a framework for implementation of DMAIC Six Sigma methodology for a manufacturing firm. The results presented are based on the data collected from the shop floor. Results and findings of the study were implemented for quality improvement of the process. Originality/value - The study is based on an original research conducted with the objective of quality improvement in the anodising process of the production process. Besides presenting an approach to DMAIC Six Sigma methodology, an application of the current reality tree tool for root cause analysis is presented, a tool used limitedly in the Six Sigma studies. The tool finds its uniqueness in its ability to address problems relating multiple factors than isolated factors.
机译:目的 - 本文的目的是研究便携式放大器生产过程的阳极化过程,以识别和消除变化的来源,以提高过程生产力。设计/方法/方法 - 该研究采用了定义 - 测量分析 - 改进控制(DMAIC)六西格玛方法。在DMAIC框架内,各种质量管理工具,如SIPOC分析,原因和效果图,当前现实树等,用于不同阶段。调查结果 - 发现高拒绝率是导致该过程生产力降低的主要问题。将四种类型的缺陷被确定为基线过程中拒绝的主要原因。帕累托分析导致检测顶部缺陷,然后详细分析,以找到问题的根本原因。进一步的研究导致在实施之前找到了与管理层讨论的改进措施。再次对该过程进行采样以检查改进,并建立控制措施。实际意义 - 该研究为制造公司实施了DMAIC六西格玛方法的框架。提出的结果基于从车间收集的数据。研究了该研究的结果和调查结果以质量改进的过程。原创性/价值 - 该研究基于以生产过程的阳极阳性化的质量改善而进行的原始研究。除了呈现DMAIC六种Sigma方法的方法外,还提出了用于根本原因分析的当前现实树工具,该工具在六种Sigma研究中使用。该工具在其唯一性中找到了与孤立因素相关的多因素相关的问题。

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