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RECONSTRUCTION OF THE BOILER SECTION OF A DRY COKE QUENCHING PLANT

机译:干焦淬火厂沸腾段的改造

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In 1979, a dry coke quenching system was built as part of coking battery No. 5 at Kemerovo Coke and Chemical Plant, which consisted of four units for quenching coke containing KST-80-1 recycling boilers produced by the Belenergomash boiler plant (Belgorod). Boiler parameters: Steam pressure at outlet, kgf/cm~2 40 Temperature of steam from superheater, deg C 440 Boiler throughout, t/h 25 To convert the parameters of the steam from the boilers to those of the steam used in the technology, in the DCQS were mounted four reduction and cooling units (RCU) type 40/6, which reduced the steam pressure from 40 to 6 kgf/cm~2. As the other boilers at the plant produce steam with a pressure of 13-14 kgf/cm~2 at a temperature of 300 deg C, and also because it was not necessary to use high-parameter steam from the DCQS boilers, in 2001 experts from the Coke Company proposed to modify the DCQS boilers to convert them to reduced parameters. Also, to produce high-pressure steam from these boilers, use was made of a group of PE-150-63 pumps providing a pressure of 64 kgf/cm~2 (4AZM-500 electric motors of power 500 kW, 6000 V). To implement this, the power engineers at the Coke Company worked with experts at the Sibenergomash Boiler Company (Barnaul) on converting the KST-80-1 boilers to reduced parameters. The designers at the Sibenergomash Company did the necessary calculations and produced the documentation to modify the boilers. The calculations also envisaged increasing the throughput of the boilers by 2-3 t/h of steam, which was very valuable to the Coke Company because of an ongoing deficiency of heat energy in the winter.
机译:1979年,克麦罗沃焦炭和化工厂的5号炼焦电池组建成了干式焦炭淬火系统,该系统由四个单元组成,用于淬灭含有Belenergomash锅炉厂(别尔哥罗德)生产的KST-80-1再循环锅炉的焦炭。锅炉参数:出口蒸汽压力,kgf / cm〜2 40过热器的蒸汽温度,℃440锅炉整体温度,t / h 25要将锅炉的蒸汽参数转换为该技术中使用的蒸汽参数,在DCQS中安装了四个40/6型减压和冷却单元(RCU),将蒸汽压力从40 kgf / cm〜2降至6 kgf / cm〜2。由于工厂中的其他锅炉在300摄氏度的温度下产生的压力为13-14 kgf / cm〜2的蒸汽,并且还因为没有必要使用DCQS锅炉的高参数蒸汽,因此2001年的专家来自可口可乐公司的提议是修改DCQS锅炉,将其转换为简化的参数。同样,为了从这些锅炉中产生高压蒸汽,使用了一组压力为64 kgf / cm〜2的PE-150-63泵(功率为500 kW,6000 V的4AZM-500电动机)。为此,可口可乐公司的电力工程师与Sibenergomash锅炉公司(Barnaul)的专家合作,将KST-80-1锅炉转换为简化的参数。 Sibenergomash公司的设计人员进行了必要的计算,并编制了文档以修改锅炉。计算还设想将锅炉的吞吐量提高2-3吨/小时的蒸汽,这对可口可乐公司来说是非常有价值的,因为冬季热能持续不足。

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