首页> 外文期刊>Journal of Performance of Constructed Facilities >Forensic Investigation of Deteriorated Concrete in Plantation East Culverts, City of Benbrook, Texas
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Forensic Investigation of Deteriorated Concrete in Plantation East Culverts, City of Benbrook, Texas

机译:德克萨斯州本布鲁克市东涵洞人工林退化混凝土的法医调查

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摘要

Two underground concrete box culverts were installed below ground on Plantation Drive in the City of Benbrook, Texas, in 1991. The culverts consisted of precast segments with case-in-place (CIP) collars/bends. The concrete started deteriorating and spalling at several CIP bend locations as early as 1993. The concrete continued to deteriorate over the subsequent years. An investigation was launched herein to determine the cause and extent of the concrete degradation. The geotechnical investigation involved resistivity imaging, soil boring, and photo-ionic detection for exploring any soil contamination around the culverts that may enhance the concrete deterioration. Visual inspection of the deteriorated concrete helped to examine the clear concrete cover. Concrete cores were taken and tested for strength and deterioration. No soil contamination was observed at the site. The culvert water acidity was neutral. Therefore, the contamination in the underground tunnel/box culvert may not be related to the soil contamination or leakage from sewerage pipes around the culvert areas. The collected concrete core inspection and testing showed that most of the bend concrete is badly deteriorated. Although the strength of some of the more intact bends is acceptable, most of the bend concrete simply does not have sufficient strength, integrity, and ductility to effectively carry the service loads imparted on them. The rebars inside the cores were extensively deteriorated and lost much of their strengths and ductility. The visual inspection showed that the insufficient clear covers were used in the culvert wall and the slab;;this was the likely cause of the premature concrete deterioration. On the basis of the investigation performed herein, immediate rehabilitation steps were recommended.
机译:1991年,在得克萨斯州本布鲁克市的Plantation Drive上,地下安装了两个地下混凝土箱形涵洞。这些涵洞由预制预制节组成,并带有原位(CIP)项圈/弯头。早在1993年,混凝土在几个CIP弯头位置就开始恶化和剥落。在随后的几年中,混凝土继续恶化。本文开始进行调查以确定混凝土降解的原因和程度。岩土工程研究涉及电阻率成像,土壤钻孔和光电检测,以探索涵洞周围的任何土壤污染,这些污染可能会加剧混凝土的劣化。目视检查变质的混凝土有助于检查干净的混凝土覆盖层。取出混凝土芯并进行强度和劣化测试。在现场未观察到土壤污染。涵洞水的酸度为中性。因此,地下隧道/箱形涵洞中的污染可能与涵洞周围的土壤污染或污水管道的泄漏无关。收集的混凝土芯检查和测试表明,大多数弯曲混凝土严重劣化。尽管一些较完整的弯头的强度是可以接受的,但是大多数弯头混凝土根本没有足够的强度,完整性和延展性来有效地承受施加在其上的服务载荷。芯子内部的钢筋被严重损坏,失去了很多强度和延展性。目视检查表明,在涵洞壁和楼板中没有使用足够的透明覆盖层;这可能是混凝土过早老化的原因。根据此处进行的调查,建议立即采取康复措施。

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