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Failure Analysis to Directional Control Pedal Assemblies of a Crashed Helicopter

机译:坠毁的直升机方向控制踏板组件的失效分析

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摘要

In investigation to a helicopter crash accident, a pedal for pilot's yaw control input was found to be separated from pedal pivot arm by fracture through two fillet welds. Fractographic and metallurgical studies were carried out on these two welds. Fatigue striations on the fracture surfaces of the welds were found and the failure was determined to be result of fatigue of the two welds. Furthermore, weld defects including insufficient weld leg, incomplete fusion, overlap on the base metal and porosity were found and evaluated against applicable standards. It was concluded that the welds were not in compliance with the standards and are root cause of the fatigue fracture. Recommendations of revising manufacturer's production specification and/or redesigning the assembly were made.
机译:在调查直升机坠毁事故时,发现飞行员的偏航控制输入踏板通过两次角焊缝断裂而与踏板枢轴臂分离。在这两个焊缝上进行了分形和冶金研究。在焊缝的断裂面上发现了疲劳条纹,并且将故障确定为这两个焊缝疲劳的结果。此外,还发现了焊缝缺陷,包括焊脚不足,熔合不完全,母材重叠和气孔,并根据适用标准进行了评估。结论是,焊缝不符合标准,是疲劳断裂的根本原因。提出了修改制造商生产规格和/或重新设计组件的建议。

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