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首页> 外文期刊>World Oil >DNV report: Trapped drill pipe caused Macondo BOP failure
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DNV report: Trapped drill pipe caused Macondo BOP failure

机译:DNV报告:被困的钻杆导致Macondo BOP失败

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A report prepared by US Det Norske Veritas (DNV) Columbus, the contractor that performed the examination of the blowout preventer on the Macondo well, has been made available to the public. According to the report, "The primary cause of failure was identified as the blind shear rams (BSRs) failing to close completely and seal the well due to a portion of drill pipe becoming trapped between the ram blocks. The position of the drill pipe between the upper annular and the upper variable bore rams (VBRs) led to buckling and bowing of the drill pipe within the wellbore. Once buckling occurred, the BSRs would not have been able to completely close and seal the well. The buckling most likely occurred on loss of well control." The BSRs were unable to move the entire drill pipe cross-section into the shearing surfaces of the blades, and during the shearing process, the pipe was deformed outside the shearing blade surfaces.
机译:由美国Det Norske Veritas(DNV)哥伦布公司(在Macondo井上进行防喷器检查的承包商)编写的报告已向公众公开。根据报告,“故障的主要原因是盲剪切闸板(BSR)由于钻杆的一部分被夹在闸板块之间而无法完全关闭和密封井。上部环形钻头和上部可变孔夯(VBR)导致井筒内钻杆发生屈曲和弯曲,一旦发生屈曲,BSR将无法完全关闭并密封井眼。失去良好的控制。” BSR无法将整个钻杆横截面移动到刀片的剪切表面,并且在剪切过程中,管道在剪切刀片表面的外部变形。

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