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Hot metal desulphurising: Redesigning the hot metal ladle lining at the Corus IJmuiden BOS plant no.2

机译:铁水脱硫:在Corus IJmuiden BOS 2号工厂重新设计铁水包衬

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The transfer of hot metal desulphurising from the torpedo cars to the hot metal ladles at the Umuiden BOS plant no.2 caused a decrease in ladle lining life from 680 to 470 heats. Changing the desulphurising agent CaC2 for CaO during a trial period, for environmental reasons, led to a further decrease in refractory life. Availability of the ladles became critical and the major reasons for the low life were identified. Solving one of them, temperature, quickly resulted in restoration of the original lives. However, re-introduction of the new desulphurising agent on 50 percent of the heats again resulted in a decrease, this time from 700 to 550 heats. In order to be prepared for the full introduction of the new agent, thorough investigation of worn linings was conducted. The investigation revealed the major (chemical) wear mechanisms and with these findings, a new design for the hot metal ladle was proposed. The initial trial results with the new ASC lining are promising.
机译:Umuiden BOS 2号工厂从鱼雷车将脱硫的铁水转移到铁水包中,导致钢包衬里寿命从680炉减少到470炉。在试验期间,出于环境原因而将脱硫剂CaC2更改为CaO,导致耐火材料寿命进一步缩短。钢包的可用性变得至关重要,并且确定了寿命低的主要原因。解决其中之一温度问题很快恢复了原始生活。但是,在50%的热量上重新引入新的脱硫剂又导致热量减少,这次是从700到550。为了准备完全引入新剂,对磨损的衬里进行了彻底的调查。调查揭示了主要的(化学)磨损机理,并根据这些发现提出了一种针对铁水钢包的新设计。新的ASC衬里的初步试验结果很有希望。

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