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Controlled Blasting at Parsa East & Kanta Basan Opencast Mines for Safe and Efficient Mining Operations

机译:东帕萨和坎塔巴桑露天矿的受控爆破,以确保安全高效的采矿作业

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The mining industry is heading towards a technology driven optimization process, international market pressures and competitiveness ensure that this process will continue and accelerate in this century too. The development and advancement of innovative technologies are essential for the mining industry to he cost effective so that information can flow hack into the process for continuous improvement. Close on the heels the last decade has also seen a dramatic progress in the advancement of blasting technology and the quality and performance of products. Monitoring instruments, measurement technologies and computing tools now have been the capabilities of broad assumption. The performance and reliability of explosives and initiation systems are now at level that allows the distribution and sequencing of explosive energy to be carefully controlled. Blasting performance is determined by the interaction of the detonation products of an explosive and confining rock mass. Rock mass properties dominate this process. The blasting engineer is, therefore, faced with the challenge of determining which rock mass properties most influence blasting performance in each situation and of deciding how blast designs should be changed to suit different geological conditions. The measured response of residential structures is a critical indicator of troublesome or potentially damaging ground vibrations. The study involved 22 blasts, employing signature hole blast to production blasts. The bench height varied from 4 m to 6 m, and boreholes were loaded with SME explosives and in few blasts with cartridges explosives. The number of holes varied from 22 to 63 at overburden benches whereas in coal benches 14 to 21 holes were fired in a blasting round. The total explosive weight fired in a round varied between 250 kg to 1575 kg and the explosive weight per delay also varied from 24 kg to 95 kg. The quality test of nonel tubes were performed and in-the-hoie VOD of explosives were tested for optimisation of blast design. The delay timing between the rows were optimised in view of proper rock face movement by performing signature blast in the overburden bench to avoid the overlapping of blast vibration waves and accordingly blast designs were optimised which yielded desired blast results.
机译:采矿业正在朝着技术驱动的优化过程前进,国际市场的压力和竞争力确保了该过程在本世纪也将继续并加速发展。创新技术的发展和进步对采矿业而言至关重要,因为它具有成本效益,因此信息可以流入流程以进行持续改进。近十年来,爆破技术,产品质量和性能的进步也取得了巨大进步。监视仪器,测量技术和计算工具现已成为广泛假设的功能。现在,炸药和起爆系统的性能和可靠性处于可精确控制炸药能量分配和排序的水平。爆破性能取决于炸药和围岩的爆炸产物的相互作用。岩体特性主导了这一过程。因此,爆破工程师面临的挑战是确定每种情况下哪种岩体特性对爆破性能的影响最大,并决定应如何更改爆破设计以适应不同的地质条件。住宅结构的测量响应是麻烦或潜在破坏性地面振动的关键指标。该研究涉及22起爆炸,采用标志性孔道爆炸来生产爆炸。工作台高度从4 m到6 m不等,钻孔中装有SME炸药,少数爆炸中装有弹药。在覆盖层工作台中,孔的数量从22到63不等,而在煤炭工作台中,在一轮爆破中开了14至21个孔。一轮发射的炸药总重量在250公斤到1575公斤之间,每次延迟的炸药重量也从24公斤到95公斤不等。进行了诺埃尔管的质量测试,并测试了炸药的现场VOD,以优化爆炸设计。考虑到适当的岩面运动,通过在覆盖层台阶上进行标志性爆破以避免爆破振动波的重叠来优化行之间的延迟时间,因此优化了爆破设计,从而产生了理想的爆破效果。

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