首页> 外文期刊>Journal of the Chinese Institute of Environmental Engineering >TREATMENT OF GASEOUS VOLATILE ORGANIC COMPOUNDS IN ACTIVATED SLUDGE SYSTEM
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TREATMENT OF GASEOUS VOLATILE ORGANIC COMPOUNDS IN ACTIVATED SLUDGE SYSTEM

机译:活性污泥系统中气态挥发性有机物的处理

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摘要

An activated sludge aeration tank (W x L x H = 40 x 40 x 300 cm) with a set of 2 mm orifice air spargers was utilized to treat gas-borne volatile organic compounds (VOCs, toluene, p-xylene, and dichloromethane) in air streams. Effects of liquid depth, aeration intensity (G/A), overall mass transfer coefficient of oxygen in clean water (K_La_(O_2)) dimensionless Henry's law coefficient of the tested VOC (H), and the influent gaseous VOC concentration (C_0) on the efficiency of the VOC removal were examined and compared with a literature-cited model. Results show that the measured VOC removal efficiencies and those predicted by the model were comparable at a G/A of 3.75-11.25 m~3 m~(-2) h~(-1) and C_0 of around 1-6 mg L~(-1). Experimental data also indicate that the reactor with K_La_(O_2)= 5-15 h~(-1) could achieve > 85% removal of VOCs with H = 0.24-0.25 at an aerated liquid depth of 1 m, and > 95% removal of dichloromethane with H = 0.13 at a liquid depth of 1 m.
机译:带有一组2 mm孔口空气喷射器的活性污泥曝气池(宽x长x高= 40 x 40 x 300厘米)用于处理气体传播的挥发性有机化合物(VOC,甲苯,对二甲苯和二氯甲烷)在气流中。液体深度,通气强度(G / A),净水中氧气的总传质系数(K_La_(O_2))无量纲的被测VOC亨利定律系数(H)和进水气态VOC浓度(C_0)的影响检查了VOC去除效率,并与文献引用的模型进行了比较。结果表明,在3.75-11.25 m〜3 m〜(-2)h〜(-1)的G / A和C_0约为1-6 mg L〜的情况下,测得的VOC去除效率与模型预测的相当。 (-1)。实验数据还表明,在充气深度为1 m的情况下,K_La_(O_2)= 5-15 h〜(-1)的反应器可以实现H2> 0.24-0.25时VOC的去除率> 85%,H = 0.24-0.25。在1 m的液体深度下用H = 0.13溶解的二氯甲烷。

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