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首页> 外文期刊>Journal of bridge engineering >Assessment of Performance of Seismic Isolation System of Bolu Viaduct
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Assessment of Performance of Seismic Isolation System of Bolu Viaduct

机译:博卢高架桥隔震系统性能评估

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摘要

The Bolu viaduct is a 2.3-km-long seismically isolated structure that was nearly complete when it was struck by the 1999 Duzce earthquake in Turkey. It suffered complete failure of the seismic isolation system and narrowly avoided total collapse due to excessive superstructure movement. This paper presents an evaluation of the design of the viaduct's seismic isolation system and an assessment of its performance in the Duzce earthquake. Evaluation of the seismic isolation system's design has revealed that it did not meet the requirements of the AASHTO Guide Specifications for Seismic Isolation Design. Analysis of the viaduct with motions sealed in accordance with the AASHTO Guide Specifications resulted in a displacement demand of 820 mm, which is far more than the 210 rnm displacement capacity of the existing isolation system. Analysis of the viaduct for a simulated near-fault motion with characteristics consistent with the site conditions resulted in an isolation system displacement demand of 1,400 mm. This indicates that, even if the isolation system had been designed in compliance with the AASHTO, it would have still suffered damage in the earthquake.
机译:博卢高架桥是一个2.3公里长的地震隔离结构,在1999年土耳其杜兹地震中被撞时几乎已经完成。它遭受了地震隔离系统的完全破坏,并避免了由于过度的上部结构移动而导致的整体倒塌。本文对高架桥的隔震系统设计进行了评估,并评估了其在Duzce地震中的性能。对隔震系统设计的评估表明,它不符合《 AASHTO隔震设计指南规范》的要求。根据AASHTO指南规范对高架桥进行密封运动的分析得出位移需求为820 mm,这远远超过了现有隔离系统的210 rnm位移能力。分析高架桥的模拟近断层运动具有与现场条件一致的特性,导致隔离系统位移需求为1,400 mm。这表明,即使隔离系统的设计符合AASHTO的规定,它在地震中仍然会遭受破坏。

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