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Operational experience on a grid connected 100 kWe biomass gasification power plant in Karnataka, India

机译:印度卡纳塔克邦并网的100 kWe生物质气化发电厂的运营经验

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摘要

The paper reports the operational experience from a 100 kWe gasification power plant connected to the grid in Karnataka. Biomass Energy for Rural India (BERI) is a program that implemented gasification based power generation with an installed capacity of 0.88 MWe distributed over three locations to meet the electrical energy needs in the district of Tumkur. The operation of one 100 kWe power plant was found unsatisfactory and not meeting the designed performance. The Indian Institute of Science, Bangalore, the technology developer, took the initiative to ensure the system operation, capacity building and prove the designed performance. The power plant connected to the grid consists of the IISc gasification system which includes reactor, cooling, cleaning system, fuel drier and water treatment system to meet the producer gas quality for an engine. The producer gas is used as a fuel in Cummins India Limited, GTA 855 G model, turbo charged engine and the power output is connected to the grid. The system has operated for over 1000 continuous hours, with only about 70 h of grid outages. The total biomass consumption for 1035 h of operation was 1111 at an average of 107 kg/h. Total energy generated was 80.6 MWh reducing over 1001 of CO_2 emissions. The overall specific fuel consumption was about 1.36 kg/kWh, amounting to an overall efficiency from biomass to electricity of about 18%. The present operations indicate that a maintenance schedule for the plant can be at the end of 1000 h. The results for another 1000 h of operation by the local team are also presented.
机译:该论文报告了连接到卡纳塔克邦电网的100 kWe气化发电厂的运行经验。印度农村生物质能能源计划(BERI)是一项实施气化发电的计划,其装机容量为0.88 MWe,分布在三个位置,以满足Tumkur地区的电能需求。发现一台100 kWe的电厂的运行情况不理想,未达到设计的性能。印度科学研究院(班加罗尔)是技术开发人员,它主动确保系统运行,能力建设并证明设计的性能。连接到电网的发电厂由IISc气化系统组成,该系统包括反应器,冷却,清洁系统,燃料干燥器和水处理系统,以满足发动机的生产者用气质量。天然气在康明斯印度有限公司GTA 855 G型,涡轮增压发动机中用作燃料,功率输出连接到电网。该系统已连续运行1000多个小时,仅发生了约70小时的电网中断。运转1035小时的总生物量消耗为1111,平均107 kg / h。产生的总能量为80.6 MWh,减少了超过1001的CO_2排放。总体比燃料消耗约为1.36千克/千瓦时,相当于从生物质到电力的总效率约为18%。当前的操作表明,该工厂的维护计划可以在1000小时结束时进行。还显示了当地团队再运行1000小时的结果。

著录项

  • 来源
    《Energy for sustainable development》 |2011年第3期|p.231-239|共9页
  • 作者单位

    Centre for Sustainable Technologies, Indian Institute of Science Bangalore, India;

    Combustion Gasification and Propulsion Laboratory, Dept of Aerospace Engineering, Indian Institute of Science Bangalore, India;

    Combustion Gasification and Propulsion Laboratory, Dept of Aerospace Engineering, Indian Institute of Science Bangalore, India;

    Combustion Gasification and Propulsion Laboratory, Dept of Aerospace Engineering, Indian Institute of Science Bangalore, India;

    Biomass Energy for Rural India, Indian Institute of Science Bangalore, India;

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  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

    distributed power generation; grid connection; biomass gasification system; rural energy;

    机译:分布式发电;电网连接;生物质气化系统;农村能源;

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