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Defect reduction for fabric cutting process to produce polo shirts : a case study of garment factory

机译:减少生产POLO衫的面料切割过程中的缺陷:以服装厂为例

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This research aims to study the factors affecting the crooked fabric cutting and to present the new cuttingprocedure that complies with the factors affecting the crooked fabric cutting of a case study. The defect infabric cutting process was crooked fabric making nonconforming product. The cause and effect diagramwas utilized to analyze and suggest related factors leading to the problem. It was showed that the number oftimes of knife sharpening and the number of layers in fabric paving would affect the crooked fabric cuttingthe design of experiment was applied to determine appropriate the level of these factors. The main factorsignificantly affected the crooked fabric cutting (p & 0.05) was the number of times of knife sharpening, but the number of layers in fabric paving and interaction between both factors would not significantly affect thecrooked fabric cutting. The number of times of knife sharpening in the level 4 had been sharpened twentytimes in each cutting round. The least average defective proportion was 0.0173. Then the new cuttingprocedure would significantly reduce average defective proportion. It could reduce the average number ofdefective items as 5.74 pieces in each cutting round or 70.52 percents.
机译:这项研究旨在研究影响弯曲织物切割的因素,并提出一种新的切割程序,该程序符合影响弯曲织物切割的因素的案例研究。织物切割过程中的缺陷是弯曲的织物,使产品不合格。利用因果图来分析和建议导致问题的相关因素。结果表明,磨刀次数和铺路层数会影响弯曲的织物切割效果。通过实验设计确定了这些因素的适当水平。影响弯曲织物切割的主要因素(p <0.05)是刀的锐化次数,但是织物铺路中的层数以及这两个因素之间的相互作用不会显着影响弯曲织物的切割。在每个切割回合中,级别4中的磨刀次数已被磨锐20次。最小的平均缺陷率为0.0173。然后,新的切割程序将大大降低平均缺陷率。这样可以将平均缺陷数量减少为每个切割回合中的5.74件,即70.52%。

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