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Failure analysis of leakage caused by perforation in an L415 steel gas pipeline

机译:L415煤气管道穿孔引起泄漏的失效分析。

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The reasons for the failure of a buried pipeline perforated during construction were investigated by a chemical composition analysis; a metallographic test; macromorphology observation; characterization of the corrosion products by scanning electron microscopy, energy-dispersive X-ray spectroscopy, and X-ray diffraction; field medium characterization; and an analysis of the working conditions. The results revealed that the material composition and organization of the steel pipe conformed to API Specification 5CT. However, the reason for the perforation of the L415 steel pipe was an ultrahigh growth rate of pitting corrosion, as high as 14mm per year. We confirmed that the synergistic effect of a high partial pressure of oxygen introduced by an improper packing process and concentrated Cl?in the corrosion product layer, which originated from groundwater with a high salt concentration that was used for the water pressure test, were responsible for the failure process.
机译:通过化学成分分析研究了在施工过程中穿孔的地下管道发生故障的原因。金相测试;宏观形态观察通过扫描电子显微镜,能量色散X射线光谱和X射线衍射表征腐蚀产物;现场介质表征;并分析工作条件。结果表明,钢管的材料组成和组织符合API规范5CT。但是,L415钢管穿孔的原因是点蚀的超高增长率,每年高达14mm。我们确认,由不适当的填充过程引入的高氧分压和腐蚀产物层中浓的Cl?的协同作用是由水压力试验所用的高盐浓度地下水引起的。失败过程。

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