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Investigation of a large ground collapse and countermeasures during mountain tunnelling in Hangzhou: a case study

机译:杭州山区隧道大地面塌方调查及对策研究

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摘要

This paper presents a case study of ground collapse (30m wide and 16m deep) during tunnelling under a water channel in the city of Hangzhou, China. The ground collapse damaged the constructed tunnel locally, and remedial measures had to be taken to resume the tunnelling works. In this paper, a forensic geotechnical and geological study was undertaken in which the geological condition at the collapsed site was reviewed, the causes for the collapse were investigated, and the development of the soil failure mechanism was evaluated. Remediation measures undertaken at the project site are also discussed. During this forensic investigation study, the strata over the tunnel was found to be of low strength and furthermore erodible to groundwater seepage. Groundwater seepage was detected, which was attributed to be the triggering force that contributed to the collapse. Tunnelling construction using explosives for blasting rocks was attributed to be one of the causes of the failure. A four-step rapid remediation measure was proposed on site, which included filling of the collapsed crater, reinforcement of collapsed debris in the tunnel, grouting and dewatering, and removal of debris and tunnelling. Tunnelling was resumed soon thereafter. The field monitoring data validated effectiveness of the proposed rapid remediation.
机译:本文以中国杭州市某水道下的隧道开挖过程中地面塌陷(宽30m,深16m)为例。地面塌方在当地破坏了已修建的隧道,因此必须采取补救措施以恢复隧道工程。本文进行了法医岩土和地质研究,审查了塌方的地质条件,调查了塌方的原因,并评估了土壤破坏机理的发展。还讨论了在项目现场采取的补救措施。在此法证调查研究中,发现隧道上方的地层强度低,而且容易被地下水渗漏。地下水渗漏被发现,这是造成塌陷的触发力。使用炸药进行岩石爆破的隧道施工被认为是失败的原因之一。现场提出了四步快速补救措施,其中包括填满坍塌的火山口,加固隧道中塌陷的碎屑,注浆和脱水以及清除碎屑和隧穿。此后不久恢复了隧道传输。现场监测数据验证了所建议的快速补救措施的有效性。

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  • 作者单位

    Shanghai Jiao Tong Univ, State Key Lab Ocean Engn, Shanghai 200240, Peoples R China|Collaborat Innovat Ctr Adv Ship & Deep Sea Explor, Shanghai 200240, Peoples R China|Shanghai Jiao Tong Univ, Sch Naval Architecture Ocean & Civil Engn, Dept Civil Engn, Shanghai 200240, Peoples R China;

    Shanghai Jiao Tong Univ, State Key Lab Ocean Engn, Shanghai 200240, Peoples R China|Collaborat Innovat Ctr Adv Ship & Deep Sea Explor, Shanghai 200240, Peoples R China|Shanghai Jiao Tong Univ, Sch Naval Architecture Ocean & Civil Engn, Dept Civil Engn, Shanghai 200240, Peoples R China|Swinburne Univ Technol, Dept Civil & Construct Engn, Hawthorn, Vic 3122, Australia;

    Univ Victoria, Dept Civil Engn Engn & Comp Sci ECS, 424,3800 Finnerty Rd, Victoria, BC V8P 5C2, Canada;

    Swinburne Univ Technol, Dept Civil & Construct Engn, Hawthorn, Vic 3122, Australia;

    Shanghai Jiao Tong Univ, Sch Naval Architecture Ocean & Civil Engn, Dept Civil Engn, Shanghai 200240, Peoples R China;

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  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

    Tunnelling; Ground collapse; Seepage; Rapid remediation; Case study;

    机译:隧道;地面塌陷;渗流;快速修复;案例研究;
  • 入库时间 2022-08-18 04:22:38

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