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Alternators

机译:交流发电机

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摘要

The alternator suffered a total mechanical failure after only 144.7 hours. The replacement unit failed after only 41.8 hours in service. Observation suggests the alternator case hardware was not properly torqued and/or was not assembled with locking fluid. Each failure found the aircraft in near-IMC conditions. Alternator failed to charge during cross-country flight. Inspection shows separation of alternator case halves, resulting in sloppy tolerance on drive shaft main bearing and failure to produce current. While airborne, the #2 alternator (p/n 653344) was inoperative. Investigation discovered the alternator's field was open. During replacement, maintenance noted the cooling fan was covered with a dusting of copper-colored particles, which could be from the brush slip rings.
机译:只有144.7小时后,交流发电机遭受了总机械故障。 替换单元仅在服务中只有41.8小时后失败。 观察表明交流发电机盒硬件未正确扭转和/或未与锁定流体组装。 每次故障都发现近乎IMC条件的飞机。 交流发电机在越野航班期间无法充电。 检查显示交流发电机的分离,导致驱动轴主轴承的邋且宽度,并且未能产生电流。 虽然空气传播,#2交流发电机(P / N 653344)不起作用。 调查发现了交流发电机的领域是开放的。 在更换期间,维护注意到冷却风扇被铜色颗粒的粉尘覆盖,这可能来自刷子滑环。

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  • 来源
    《Aviation safety 》 |2020年第6期| 31-31| 共1页
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