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Field Application of HCl-Formic Acid System to Acid Fracture Deep Gas WellsCompleted with Super Cr-13 Tubing in Saudi Arabia

机译:HCl-甲酸体系在酸性裂缝深层气井中的现场应用 r n沙特阿拉伯超级Cr-13管完井

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This paper describes optimization of gelled and in-situ gelledrnHCl/formic acid systems to stimulate deep gas wellsrncompleted with super Cr-13 tubing. High temperaturesrnencountered in deep wells and the susceptibility of super Cr-rn13 to severe corrosion by concentrated HCl solutions and highrnchloride ion concentrations render acid stimulation a veryrndifficult task. Therefore, extensive experimental and fieldrnstudies were performed to develop a cost effective acid systemrnto enhance the productivity of deep gas wells, whilernmaintaining the integrity of the super Cr-13 tubing.rnCoreflood tests indicated that this acid system can createrndeep wormholes in tight reservoir cores (less than 1 md).rnCorrosion tests, however, indicated that protecting super Cr-13rntubulars during pumping this acid (15 wt% HCl/9 wt% formicrnacid) is not an easy task, especially at downhole temperaturesrn(275oF). A very limited number of inhibitor aids were foundrnto be effective in protecting super Cr-13 at reservoirrnconditions. To optimize the corrosion inhibitor package, thernbottom hole temperature was measured in a few wells duringrnacid injection.rnBased on lab tests and field measurements, an acidrntreatment was designed and applied in the field. The treatedrnwells responded positively to the treatment. Most importantly,rnthe integrity of the super Cr-13 was maintained. This wasrnconfirmed from chemical analysis of well flowback samplesrnfollowing the treatment and measurement of the tubing insiderndiameter before and after the treatment. The maximum Crrnconcentration in the flowback sample was less than 2 mg/L.rnMolybdenum and nickel concentrations were less than 1 mg/L.rnThe total iron concentration was less than 200 mg/L. Thisrnvalue is significantly less than that noted with wells completedrnwith low-carbon steel tubulars.
机译:本文介绍了凝胶化和原位凝胶化的HCl /甲酸体系的优化方法,以刺激使用超级Cr-13油管完井的深层天然气井。在深井中遇到了高温,超级Cr-rn13对浓盐酸溶液和高氯离子浓度的严重腐蚀的敏感性使酸增产变得非常困难。因此,进行了广泛的实验和现场研究,以开发一种成本有效的酸体系,以提高深层气井的生产率,同时保持Cr-13超级油管的完整性。岩心驱油测试表明,该酸体系可在致密的储层岩心中形成深虫洞(较少然而,腐蚀试验表明,在泵送这种酸(15 wt%HCl / 9 wt%甲酸)的过程中,保护超级Cr-13空心管并非易事,尤其是在井下温度rn(275oF)时。发现在储藏条件下,非常有限数量的抑制剂助剂可有效保护超级Cr-13。为了优化缓蚀剂包装,在注酸过程中在几个井中测量了井底温度。基于实验室测试和现场测量,设计了酸处理方法并应用于现场。处理过的孔对处理反应良好。最重要的是,超级Cr-13的完整性得以保持。处理前后对油井内径进行处理和测量后,对井内回流样品进行了化学分析,证实了这一点。返排样品中的最大Crrn浓度小于2 mg / L。钼和镍的浓度小于1 mg / L。rn总铁浓度小于200 mg / L。该值明显小于用低碳钢管完成的井所记录的值。

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